NS OPERATING EXPERIENCE WEEKLY SUMMARY 93-10 March 5 - March 11, 1993 The purpose of the NS Operating Experience (OE) Weekly Summary is to enhance safety throughout the DOE complex by promoting feedback of operating experience and encouraging the exchange of information among DOE nuclear facilities. The OE Weekly Summary is distributed for information only. No specific actions or responses are required solely as a result of this document. Readers are cautioned that review of the OE Weekly Summary should not be relied upon as a substitute for a thorough review of the interim and final Occurrence Reports. The following events were reviewed during the week of March 5 - 11, 1993. ITEM PAGE 1. DIESEL GENERATOR FAILS TO START DURING TEST 1 2. PROCEDURE VIOLATION BY FIRE WATCHER 2 3. MISSING INSTRUMENT CHECK SOURCE 3 4. LOW FLASHPOINT OF DIESEL FUEL OIL 3 5. CAUTION REGARDING THE PACKAGING OF METALLIC URANIUM IN STEEL DRUMS 4 6. INCORRECT CIRCUIT BREAKER OPERATION CAUSES REACTOR TRIP BREAKERS TO OPEN 5 7. OPERATIONAL SAFETY REQUIREMENT VIOLATION CAUSED BY FAILED TANK LEVEL INSTRUMENTATION 6 8. INADVERTENT LIQUID WASTE TRANSFERS 6 9. RADIOACTIVE DISCHARGE FROM SHUTDOWN FACILITY 7 10. PERSONNEL INADVERTENTLY DISCONNECT FUEL HANDLING UNIT FROM HOOK 8 FINAL REPORTS - SUMMARIES 1. FAILURE OF REACTOR COARSE LEVEL INDICATION 9 1. DIESEL GENERATOR FAILS TO START DURING TEST On March 5, 1993, in the Laboratory Technical Area (LTA) at Savannah River, operations personnel were unable to perform a no-load start test on the 792-A Sand Filter Diesel Generator. The LTA is the general research and development laboratory for the entire Savannah River Site and handles many hazardous substances. The diesel generator provides emergency power to maintain the exhaust flow through the sand filter in the event of a facility loss of power. The Sand Filter is a large (100' x 150') underground structure downstream from the HEPA filters. It is intended to provide a last barrier to filter air that may contain radioactive isotopes. Failure of facility power combined with the failure of the diesel generator could cause ventilation problems in the 773A facility, where many glove boxes and hot cells are in use, and could result in spreading contamination throughout the facility and possibly into the environment (ORPS REPORT SR--WSRC-LTA-1993-0014). The initial investigation erroneously concluded that the battery did not have sufficient cranking power to start the diesel. The investigators knew that the battery was fairly old and was scheduled for replacement soon, although it still met the minimum specification requirements for the system. The batteries were recharged for two hours on a trickle charger, but the diesel still would not start. The batteries were then warmed to increase their efficiency, and a diesel starting fluid was injected into the diesel's air intake to assist starting, but the unit still would not start. Maintenance and engineering personnel found the damper on the air intake line was unable to open, as required for normal operation. The problem was not noticed when investigators used the diesel starting fluid, because they injected the fluid into the intake piping at a point downstream of the stuck damper. The damper was opened and the unit started and ran without further problem. The investigation is continuing to determine whether the damper problem is mechanical or electrical. 2. PROCEDURE VIOLATION BY FIRE WATCHER On March 5, 1993, in Building 707 at Rocky Flats, a shift technical adviser found that an employee providing a continuous fire watch on the second floor of the building was not performing his required duties. The purpose of this facility is to conduct thermal stabilization operations for the Rocky Flats site, including oxidation operations of plant inventory and duct remediation. Fire watches in this facility are required to meet the Operational Safety Requirements for previously identified safety deficiencies. The main safety function of the fire watch is to cover those areas that do not have a functional automatic fire detection system. The individual was reading a magazine, and the fire watch log-sheet that documents completion of the fire watch inspections had been filled out twenty minutes in advance. The individual concerned was relieved of his duties pending the completion of the investigation (ORPS REPORT RFO--EGGR-PUFAB- 1993-0047). Facilities are encouraged to review DOE Safety Notice 92-4, "FACILITY LOGS AND RECORDS", (September 1992), by the Office of Nuclear Safety. The notice summarizes situations at DOE facilities where logs were falsified, incorrectly entered, or not completed. Readers are reminded that such practices are inconsistent with DOE requirements and guidelines. Additional related commercial industry experience is discussed in Nuclear Regulatory Commission Information Notice (IN) 92-30, "FALSIFICATION OF PLANT RECORDS." Quoting from Safety Notice 92-4, "DOE and commercial industry experience emphasizes the potential adverse impact of improper logkeeping on nuclear safety, as well as representing possible violations of Federal regulatory requirements and criminal statutes." 3. MISSING INSTRUMENT CHECK SOURCE On March 2, 1993, personnel at the Oak Ridge National Laboratory were unable to locate a 0.2 uCi thorium-232 check source, creating a potential hazard that facility personnel could be unknowingly exposed to radiation. Facility personnel were performing the semi-annual leak test of HFIR sources when they identified the source as missing. Several searches failed to locate it (ORPS Report ORO--MMES-X10ENVIOHP-1993- 0002). There have been many instances at DOE facilities of improper disposal and loss of control of radioactive sources. On December 22, 1992, personnel at the Chem- Nuclear Geotech facility discovered an uncontrolled cobalt-60 source on the ground outside the Source Storage Building at the Grand Junction Project Office during a routine weekly survey. Dose rates from the source were 220 millirems/hour on contact. Facility personnel verified that the site did not have a source of this type in inventory, but a review of records indicated that a cobalt-60 source had been reported missing in 1970 (ORPS Report ALO--GEO-GJO-1992-0019). Another loss of source accountability occurred on July 22, 1992, at a Hanford facility when a cesium-137 check source used for calibration of radiation detection instruments was discovered missing. Facility personnel found the source several days later in a parking lot. The source was damaged and reading 10,000 disintegrations per minute. A Radiation Protection Technologist had used the source to demonstrate an equipment malfunction in the parking lot and the source was not properly returned to its container (ORPS Report RL--PNL-PNLBOPEM-1992-0008). NS reported on several other occurrences involving improper control and disposal of radioactive sources in OE Weekly Summary 93-06. One event involved the death of several people in China when a worker found a cobalt-60 source while cleaning a well in November 1992. In the following days, he and two members of his immediate family died of radiation sickness. In a similar case in Brazil in 1987, four people died and 240 absorbed high doses of the radioactive isotope cesium-137 when a group of children discovered a glowing capsule in a scrap heap and began to play with it. These events underscore the importance of the proper control of radioactive sources. Storage areas must be clearly identified and access controlled. Additional information associated with control of sources can be found in NRC Information Notice IN 90-47, "Unplanned Radiation Exposures to Personnel Extremities Due to Improper Handling of Highly Radioactive Sources." 4. LOW FLASHPOINT OF DIESEL FUEL OIL On February 18, 1993, personnel at the Savannah River Replacement Tritium Facility (RTF) determined that the flashpoint for the standby diesel generator fuel was below expected administrative limits, causing a potentially combustible condition and making the diesel generator inoperable. An analysis of the fuel oil indicated the flashpoint was 70 degrees Fahrenheit, compared to the administrative limit of 125 degrees Fahrenheit. Upon discovery, facility personnel locked the diesel out of service, barricaded the diesel generator building, and set up a blower to force fresh air into the building. Facility personnel had not determined the cause of the low flashpoint when this OE Weekly Summary was prepared. They suspect that the off-site fuel delivery service did not properly flush the tank prior to filling it with the diesel fuel scheduled for delivery to the RTF facility. If the previous shipment had been at a lower flashpoint, residual amounts may have contaminated the RTF shipment and lowered the flashpoint. A low flashpoint means that the fuel could detonate early in the compression cycle and potentially damage internal components of the diesel. Prior to this event, facility personnel had several problems with the diesel fuel. On February 2, 1993, facility personnel analyzed the diesel fuel in accordance with facility Technical Safety Requirements and determined that the fuel exceeded allowable limits for water content and bottom sediments. Workers drained the fuel from the storage tank and ordered replacement fuel. On February 8, 1993, workers refilled the storage tank and obtained samples of the fuel. The results of the analysis indicated bottom sediment in excess of surveillance requirement limits. Facility personnel drained several gallons from the bottom of the tank to flush the excess sediment. Subsequent analysis indicated that the bottom sediments were within surveillance requirement limits. DOE facilities have reported many other problems involving diesel fuel. Most fuel problems result from low usage rates and fuel degradation over time. The rate of degradation depends on storage temperature and the quality of the fuel. Heat may accelerate fuel degradation and cause condensate to form on the tank walls as the tank experiences a daily thermal cycle. Fuel degradation produces particulate and insoluble gum contaminants in the fuel. The particulate, gum, and condensate tend to settle at the tank bottom creating a medium for organic growth at the fuel/water interface. Anaerobic sulfate-reducing bacteria, fungus, and yeast can grow in two- phase systems containing water and diesel fuel. Removing water and contaminants from the tank bottom and limiting the amount of water and contaminants introduced with new fuel is extremely important. A fuel maintenance and testing program can control fuel quality resulting in increased reliability of the diesel. ASTM D-975, "Standard Specification for Diesel Fuel Oils," and ASTM D-4057, "Standard Practice for Manual Sampling of Petroleum and Petroleum Products," are two industry standards often used to ensure the quality of diesel fuel. NS previously discussed the importance of monitoring emergency diesel generator fuel specifications in OE Weekly Summary 92-29. Additional information can be found in NRC IE Circular 77-15, "Degradation of Fuel Oil Flow to the EDG," and IE Information Notice 87-04, "Diesel Generator Fails Test Because of Degraded Fuel." 5. CAUTION REGARDING THE PACKAGING OF METALLIC URANIUM IN STEEL DRUMS On March 3, 1993, NS received a letter from an incident investigation team at Lawrence Livermore National Laboratory (LLNL) regarding packaging of metallic uranium in steel drums. The team reviewed several incidents involving unexpected chemical reactions in steel drums holding metallic uranium. The team concluded that although the chemistry involved in the incident is well documented, the incidents and their probable causes are not common knowledge at DOE facilities. The primary incident investigated involved an event that occurred on July 13, 1992. An LLNL technician attempted to open a 30-gallon steel drum containing about 600 kg of depleted uranium rods. After removing the clamping ring, the worker used a hammer and punch to pry the lid from the drum. Suddenly, the lid flew about three feet into the air, apparently as a result of a low-grade hydrogen/oxygen reaction. Immediately, packaging material in the drum caught fire. The technician replaced the drum lid in an attempt to extinguish the fire. Facility personnel placed the drum in an overpack and transported the container to a secure location (ORPS Report SAN--LLNL-LLNL- 1992-0062). Several weeks later, facility personnel pierced the drum to determine the composition of the gas content. The analysis indicated 25 percent hydrogen and 75 percent nitrogen. The team hypothesized that a uranium/water reaction had produced uranium oxide, uranium hydride, and hydrogen gas in the drum. When the lid was removed, oxygen reacted with the uranium hydride resulting in the hydrogen/oxygen reaction and ignition of the fire in the packaging material. The LLNL investigative team concluded that using vented containers to store and ship uranium metal was more reliable than using sealed containers. The letter states that: "Although the vent provides a pathway for moisture to enter the container, it allows the oxygen content to remain normal - thus inhibiting the uranium/water reaction - and allows any hydrogen to escape. If sealed containers are to be used, attention should be paid to the nature of the gasket and the integrity of the seal it makes. Care must be taken to ensure that no source of moisture exists in a well-sealed container of uranium metal. This means no organic packing material." The letter further recommends care when opening drums of uranium metal that have been in storage. Moreover, workers should be particularly aware of tightly sealed lids because it is possible that water has been present in the drum. In February 1993, NS issued Safety Notice 93-1, Fire, Explosion, and High-Pressure Hazards Associated with Waste Drums and Containers. Copies of Safety Notice 93-1 may be obtained by contacting the Nuclear Safety Information Center at 301-903- 5011. Reference: D.H. Wood, S.A. Snowden, H.J. Howe, Jr., L.L. Thomas, D. W. Moon, H. R. Gregg and P.E. Miller, A Caution Regarding the Packaging of Metallic Uranium in Steel Drums, University of California, Lawrence Livermore Laboratory, Livermore, California, 1993. 6. INCORRECT CIRCUIT BREAKER OPERATION CAUSES REACTOR TRIP BREAKERS TO OPEN On February 3, 1993, Instrument and Control (I&C) personnel at the Calvert Cliffs commercial nuclear power plant in Maryland opened the wrong circuit breaker during maintenance activities, inadvertently causing four of nine reactor trip breakers, which are part of the plant's Reactor Protection System, to open. The reactor continued to operate throughout the event. I&C personnel were using an approved work order to replace a nuclear instrument that was part of a Reactor Protection System (RPS) cabinet. The work order, which had been reviewed by Quality Engineering and the Shift Supervisor, specified two circuit breakers to be opened to isolate the nuclear instrument. However, when workers opened the second breaker, they deenergized the entire RPS cabinet instead of just the intended instrument causing the reactor trip breakers to open. Facility personnel determined that the breaker specified in the work order was incorrect. The work order described the breaker by its identification number and did not provide an accurate description including the name of the breaker (NRC Event Number 25001). This event illustrates the need for work control documents such as procedures and work orders to include detailed information to help reduce potential errors in the work to be performed. This event might have been avoided had both the name and number of the circuit breakers been included in the work order. Additionally, the event is a reminder that workers should be sufficiently trained and qualified, both technically and in self-checking techniques, so they will be aware of and understand expected plant responses when operating equipment. 7. OPERATIONAL SAFETY REQUIREMENT VIOLATION CAUSED BY FAILED TANK LEVEL INSTRUMENTATION On March 4, 1993, a level indicator transmitter (LIT) for a tank at the Hanford Tank Farm (a group of underground tanks containing high level radioactive waste) failed, and operators were unable to measure the level in the tank within a day, resulting in a non-conformance of a facility Operational Safety Requirement (OSR) designed to assure the integrity of the tank. The tank integrity was not in jeopardy during the event because the OSR requires a minimum level of six inches when tank ventilation is flowing to prevent implosion (tank level during the event was over 200 inches) (ORPS Report RL--WHC-TANKFARM-1993-0027). Facility personnel initially attempted to repair the failed LIT, the only one for the associated tank, in time to meet the OSR requirement. When it became apparent that this would not be likely, supervisors tried to manually measure the tank level using a "zip cord" (an electrically charged cable calibrated to indicate when it contacts the surface of the tank contents). However, logistics problems and difficulties in constructing a satisfactory glovebox prevented them from obtaining the level measurement in time to satisfy the OSR requirement. Workers repaired the LIT, and facility personnel were conducting an investigation of the occurrence to determine causes, lessons learned, and necessary corrective actions. Although in this event the tank integrity was never at risk, a similar event could have more serious consequences if a critical parameter was near its limit. This event emphasizes the importance of ensuring that backup measures to ensure compliance with safety limits are readily available and can be promptly implemented when required. 8. INADVERTENT LIQUID WASTE TRANSFERS On March 5, 1993, approximately 740 gallons of liquid waste were inadvertently transferred from a receiver tank to a storage tank at the Hanford Tank Farm causing a violation of facility LCOs regarding leak detection. The violated LCO required either that remote monitoring for the leak detection systems be operable along the transfer route or that continuous manual monitoring of the leak detectors take place. To meet the LCO requirements, Westinghouse Hanford Company (WHC) assigned personnel to continuously monitor local leak detection alarms during the transfer because the alarms were not operating at manned remote locations. Later, personnel left their stations when the transfer was suspended to troubleshoot a failed air-operated valve. During troubleshooting and cycling of the air-operated valve, an agitation pump used to suspend tank waste solids and act as the transfer pump was left running to recirculate tank contents. The pump is normally run for several hours prior to a transfer to ensure that waste solids are suspended and transferred, and facility personnel allowed it to run while the transfer was suspended hoping that the air-operated valve would be repaired quickly. Workers checked the level in Tank 244-TX every four hours while the pump was running. However, a manual isolation valve in the transfer route apparently suffered a catastrophic failure between the time it was opened to start the transfer and when it was closed to stop it. Facility personnel were unaware of the failure, which created a flow path when the air-operated valve was cycled during troubleshooting. During the inadvertent transfer, personnel were not in attendance at the local leak detection alarms to meet LCO requirements. There were no transfer line leaks during the transfer. Facility personnel repaired the air-operated valve but did not repair the leaking valve because it was located in a highly contaminated valve pit. To prevent recurrence of the event, facility personnel implemented administrative controls requiring constant surveillance of local leak detection alarms and tank levels whenever the agitation pump was running (ORPS Report RL--WHC-TANKFARM-1993-0028). In a similar event at the Savannah River FB-Line (a plutonium processing facility) in December 1991, failure of a valve to remain fully closed caused an inadvertent waste transfer. Facility personnel had closed the valve but the excessive size and weight of the valve handle caused the valve to partially open. NS identified 16 other occurrences involving inadvertent waste transfers at DOE facilities during 1991-1993. Of these 16 occurrences, 12 were caused by improper procedure use or inadequate procedure content. These events illustrate the need for facility personnel to consider the possibility of equipment failures and alternate flow paths whenever motive force for a transfer is present. These events also demonstrate the importance of adequate procedural content and use when conducting waste transfers. Procedures can be used to provide guidance on identifying and monitoring alternative flowpaths. 9. RADIOACTIVE DISCHARGE FROM SHUTDOWN FACILITY On February 12 and 13, 1993, an above-normal radioactive discharge occurred from a ventilation stack at a facility at Sellafield, a nuclear fuel reprocessing and storage site in England. The discharge coincided with work on a ventilation fan in B204, which became more extensive when fan belts had to be replaced. Sellafield personnel determined that the discharge was approximately 14 percent of the annual discharge limit for the site, and the dose to the most exposed member of the general public was .04 percent of the average dose to people in the United Kingdom (UK) from natural background radiation. According to site personnel, there was no risk to the public or the environment, and discharge levels were below Ministerial reporting levels. The source of the discharge was B203, an adjoining ex-plutonium residue recovery plant, which has been shut down since the 1980s and is being prepared for decommissioning. Sellafield personnel are planning to install a new filtration system in B203 as part of decommissioning preparations. Sellafield management indicated that had such a system been in place the discharge would not have occurred. Management also indicated that much safety analysis work would be completed before decommissioning started in order to anticipate problems associated with cleaning up old facilities and provide enhanced protection to the public and the environment. Sellafield management is also utilizing techniques similar to Total Quality Management to improve the safety of facility operations. The Sellafield work force is being consulted on proposed arrangements concerning health physics monitoring service on the site. Management is examining all aspects of Sellafield operations, including health physics monitoring to determine if they are being performed in the best possible manner. These consultations and reviews have so far resulted in proposals that emphasize the importance of maintaining safety standards while, at the same time, allowing plant operators a greater role in determining how and in what order work is performed (Sellafield Newsletter, Week Ending 2/23/93). 10. PERSONNEL INADVERTENTLY DISCONNECT FUEL HANDLING UNIT FROM HOOK On March 4, 1993, in an irradiated fuel storage pool area in building CPP-603 at the Idaho National Engineering Laboratory, a hook holding a bucket containing fuel scrap inadvertently became disconnected causing a stoppage of operations and clearance of personnel from the area. Building CPP-603 is used to receive, handle and store irradiated fuel. Underwater buckets and racks contain Fuel Handling Units (FHUs) and are used to store nuclear fuel in pools in a safe configuration to avoid nuclear criticality. At the time of the occurrence, facility personnel were installing redundant rigging to the fuel-scrap bucket (estimated weight - 30 pounds) in a pool. All 154 previous installations were on full-cluster FHUs weighing about 300 pounds. Installation of redundant rigging was a corrective action in response to a prior event where corrosion of carbon-steel yokes was observed (ORPS Reports ID--WINC-ICPP-1992- 0024). In the most recent event, a yoke supported the fuel-scrap bucket by the bucket bail. The bucket bail hung from a yoke hook rigidly attached to the yoke. The yoke hook became disconnected when rigging personnel attached the rigging (consisting of stainless-steel cable, hook and turn-buckles) and pulled on the cable to remove line slack. Because of the light weight of the bucket the riggers lifted it too far, disconnecting it from the yoke hook and leaving the bucket suspended only by the redundant rigging. The hook was found disconnected during an investigation conducted after a foreman, who was performing a final configuration check using an underwater video camera, noticed the bucket rotating. Had the bucket fallen, it would have landed on the pool floor. Recovery of the bucket from that position would be significant effort. But the bucket would not create a danger of a criticality excursion because its contents are not highly reactive. The lesson of this event is the need to account for all relevant aspects of the lifting and handling methodology (ORPS Reports ID--WINC-ICPP-1993-0014). Facility personnel report that there is no danger of a criticality excursion because they maintain double contingency for criticality. They observe facility Technical Standard, requiring a minimum edge-to-edge spacing of eight inches for FHUs. Additionally, the fuel-scrap bucket is classified as non-highly reactive. This means it could be in contact with another FHU and not create a criticality excursion. A special procedure controlled the rigging operation. Abnormal and emergency procedures were in place to control contingencies that might arise. Riggers were trained and briefed prior to the job. Training included a walk through and mockup practice. Personnel followed procedures. Facility personnel have tentatively attributed the root cause of the problem to the failure to recognize the differences involved in rigging lightweight versus full-cluster FHUs. The special procedure, training, and job briefing did not account for handling lightweight FHUs. Facility personnel plan to revise the special procedure, training, and briefings to account for FHU weight differences. Also, they plan to implement continuous underwater video monitoring for future redundant rigging operations. Finally, a special recovery procedure will be implemented for the suspended bucket. FINAL REPORTS - SUMMARIES This section of the OE Weekly Summary discusses events that have been filed as Final reports on the ORPS. These events contain new or additional lessons learned that may be of interest to personnel within the DOE complex. The description of each event, its causes, and lessons learned are edited from the original ORPS final report. 1. FAILURE OF REACTOR COARSE LEVEL INDICATION Reference: ORPS Report SR--WSRC-REACK-1993-0025 On February 2, 1993, at the Savannah River K-Reactor, a tritium production facility, personnel determined that one of the redundant reactor coarse (wide-range) level indications failed. At the time of the occurrence, K-Reactor was shutdown for a cooling tower outage. Operations personnel made the failure determination after a review of a level reading recorded on the Control Room Roundsheet. The normal reading for the indicator is 19.5 feet and the Roundsheet indicated a level greater than 20 feet, i.e., off scale. Personnel initiated an investigation and verified correct transmitter valve alignment, so they then initiated a work request to repair the transmitter. Repair personnel found a calibration problem, calibrated the transmitter and returned it to service on February 22. Nine hours elapsed from the time of the initial Roundsheet recording of greater than 20 feet and the start of the investigation. During the nine-hour period, a shift change occurred. The other level indication capability remained operational while the failed transmitter was out of service. The transmitter was a Republic Model P0331E. The root and direct causes of the transmitter calibration failure were attributed to a failed or defective part. The direct cause of the delay in finding and investigating the failure was attributed to poor employee communications. Poor communications were exhibited between and within shifts. The information was not communicated to the Shift Manager on duty and, therefore, not communicated to the incoming Shift Manager. A shift order was issued to the shifts emphasizing the importance of communications, logkeeping, turnover briefing, and exercising an inquisitive attitude towards abnormal data. This occurrence emphasized the importance of good employee communications. SAFETY NOTICES UNDER DEVELOPMENT Note: The Office of Nuclear Safety encourages input related to the development of Safety Notices. If you have any questions, comments, or information concerning events or issues similar to the following, please contact Ivon Fergus, Office of Nuclear Safety at (301) 903-6364. 1. NS has identified a number of events related to the loss of annunciators and other safety-related equipment because of problems involving 120-VAC/125- VDC systems at DOE and commercial facilities. NS is reviewing potential generic problems associated with the adequacy of 120-VAC/125-VDC systems at DOE facilities. 2. NS evaluated three events associated with the temporary diesel generator at the Rocky Flats Plant, Building 707. The lessons learned from these events, particularly as they relate to the control of temporary modifications, are being considered for dissemination in an NS Safety Notice. 3. NS is developing a Safety Notice concerning problems with Uninterruptible Power Supplies (UPS). 4. NS is considering development of a Safety Notice related to control of work at electrical substations and switchyards. 5. NS is working with Lawrence Livermore National Laboratory and DOE-SF personnel to develop a Safety Notice on cracking in ventilation ducting. 6. NS is considering developing a Safety Notice related to fuel oil supplies for Emergency Diesel Generators (EDGs). 7. NS is developing a Safety Notice to address uses of independent verification for equipment positioning. SAFETY NOTICES PREVIOUSLY ISSUED Safety Notice No. 91-1, "Criticality Safety Moderator Hazards," September 1991 Safety Notice No. 92-1, "Criticality Safety Hazards Associated With Large Vessels," February 1992 Safety Notice No. 92-2, "Radiation Streaming at Hot Cells," August 1992 Safety Notice No. 92-3, "Explosion Hazards of Uranium-Zirconium Alloys," August 1992 Safety Notice No. 92-4, "Facility Logs and Records," September 1992 Safety Notice No. 92-5, "Discharge of Fire Water Into a Critical Mass Lab," October 1992 Safety Notice No. 92-6, "Estimated Critical Positions (ECPs)," November 1992 Safety Notice No. 93-1, "Fire, Explosion, and High-Pressure Hazards Associated with Waste Drums and Containers," February 1993 Copies of NS Safety Notices may be requested from: Nuclear Safety Information Center, Office of Nuclear Safety, U.S. Department of Energy, Room S161, GTN, Washington, DC 20585