NS OPERATING EXPERIENCE WEEKLY SUMMARY 93-16 April 16 - April 22, 1993 The purpose of the NS Operating Experience (OE) Weekly Summary is to enhance safety throughout the DOE complex by promoting feedback of operating experience and encouraging the exchange of information among DOE nuclear facilities. The OE Weekly Summary is distributed for information only. No specific actions or responses are required solely as a result of this document. Readers are cautioned that review of the OE Weekly Summary should not be relied upon as a substitute for a thorough review of the interim and final Occurrence Reports. The following events were reviewed during the week of April 16 - 22, 1993. ITEM PAGE 1. MISPOSITIONED RELAY CAUSES LOSS OF CRITICALITY ALARM HORN CAPABILITY 2 2. FAILURE TO PROPERLY WEAR RESPIRATOR 3 3. PERSONNEL OVEREXPOSURE FROM MISHANDLING RADIOGRAPHY SOURCE 4 4. REACTOR SCRAM WHILE PERFORMING ON-THE-JOB TRAINING 5 5. GREASE SOLIDIFICATION CAUSES MOLDED CASE CIRCUIT BREAKER FAILURE 6 6. FRENCH EXECUTIVES ON TRIAL FOR NUCLEAR ACCIDENT 7 7. COOPER-BESSEMER DIESEL GENERATOR FUEL PUMP 10CFR21 NOTIFICATION 7 8. UNABLE TO VERIFY CRITICALITY SAFETY-LIMIT COMPLIANCE 8 9. LEVEL INSTRUMENTATION INACCURACIES OBSERVED DURING NORMAL PLANT DEPRESSURIZATIONS 9 10. OPERATOR INCORRECTLY STARTS WRONG EMERGENCY DIESEL GENERATOR 10 ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES 1. WORKER CONTAMINATIONS DURING CONSTRUCTION ACTIVITIES 11 1. MISPOSITIONED RELAY CAUSES LOSS OF CRITICALITY ALARM HORN CAPABILITY On April 14, 1993, an instrument technician at Plant 9 on the Fernald Environmental Management Project (FEMP) site found a mispositioned alarm-timer relay for the radiation-detection alarm system, resulting in loss of criticality alarm-horn capability for all of Plant 9 and Plant 81, contrary to facility operational safety requirements. Automatic, remote, criticality-alarm capability was maintained to the site communications center. Local criticality-alarm capability was maintained by a warning bell and lights at the radiation alarm station inside Plant 9. Also, the capability of the site-wide emergency message system to notify personnel to evacuate the area was maintained. The technician found the relay removed from its designated position in an alarm-relay box and lying on the bottom of the box. The technician located the mispositoned relay while doing a follow-up inspection, related to a March 31 event, after restoration of plant air to a Plant 9 alarm horn. The technician installed the relay in the proper location and completed a successful functional test of the horns. Results of a prior inspection and functional test of the alarm system by radiation technicians on April 1 showed that all Plant 9 and Plant 81 radiation-detection horns were operable. The system was not designed to signal a trouble alarm for a missing relay or open relay-box door, nor was it designed for locking the door. The radiation detection alarm system is part of the site-wide, emergency-alarm system, safety class A equipment. Plant 9, a former uranium processing facility, was unoccupied and under modification to change its function to vitrification. Plant 81, a Resource Conservation and Recovery Act storage facility, was also unoccupied. Personnel report that prior material characterizations in the areas of Plant 9 and Plant 81 indicate that a criticality event there is not possible. (ORPS Report ORO-WMCO-FMPC-1993-0026) The Office of Nuclear Safety reported the March 31 event, concerning an unauthorized isolation of plant air to a Plant 9 air horn in Operating Experience Weekly Summary 93-14 (ORPS Report ORO-WMCO-FMPC-1993-0021). In that event, a Plant 9 horn was found isolated from the plant air system and the back-up supply nitrogen bottle was missing. While loss of alarm horn capability was not a concern for this event, it caused concerns because a loss of horn capability could have occurred in an area of the site where a criticality event was possible. Facility personnel have not identified the cause of the mispositioned relay. They report that radiation technicians routinely remove radiation-detection-alarm relays when troubleshooting the alarms or doing routine inspections. Also, they report that relay removal was not part of the procedures, but that technicians remove them because of prior occurrences of false activations of alarms while inspecting and troubleshooting. The technician responsible for the April 1 inspection and testing reported that he remembers removing and reinstalling the relay. Also, site personnel reported construction activity in and around Plant 9. Prior to the event, facility personnel found that the procedure used to accomplish the April 1 inspection partially duplicated the scope of another procedure, in that both included quarterly inspections. Apparently, radiation technicians used both procedures for quarterly inspections. Facility personnel had initiated action to eliminate duplication in the procedures by revising one procedure and eliminating the other. Personnel reported on planned training of radiation technicians on the procedure revision and on the importance of following procedures. Personnel also reported that training of radiation technicians on procedure revisions was standard practice. Also, as a precaution, facility personnel inspected all other radiation- detection-alarm relay boxes and found no other relays out of place. DOE Order 4330.4A, "Maintenance Management Program," provides policy, objectives, and criteria for establishment of maintenance programs. The stated objective for surveillance and preventive maintenance addresses the need for activities to ensure that equipment needed for safe and reliable facility operation is inspected, tested, and maintained to keep that equipment within design operating condition. One criteria calls for documentation to record activities performed, data collected, and, when appropriate, the "as-found" and "as-left" condition of equipment (page I-40). The Office of Nuclear Safety is developing a safety notice to address uses of independent verification for equipment positioning. 2. FAILURE TO PROPERLY WEAR RESPIRATOR On April 14, 1993, personnel at the Oak Ridge Alpha Handling facility identified a worker wearing a respirator without the required filter canisters, increasing the risk of airborne contamination exposure. Upon discovery, facility personnel discontinued work activities and escorted the worker from the contaminated area. Nasal smears and lung counts performed on the individual were negative. The worker had been trained in the proper use of respirators and had previously used this type of equipment. The worker was preparing to bag and transfer waste in a glovebox for further disposal when the incident occurred. The radiation work permit and a facility procedure for glovebox operations specified respirator use as a precautionary measure. While there is a potential for airborne activity, the area is routinely monitored and facility personnel report that no airborne activity was discovered. The worker had obtained the respirator and filter cartridges from the industrial hygienist department. Facility procedures require workers to assemble and test respirators prior to use. Although investigation of the root cause is in progress, the worker apparently forgot to properly assemble and test the respirator before initiating work in the glovebox. Serious consequences could have resulted if there had been airborne activity present. As part of immediate corrective actions, the worker was given counseling, and facility personnel suspended all activities requiring respirator use until respiratory protection refresher training could be provided to operators. In addition, quality assurance personnel plan to perform surveillances of work activities requiring respiratory protection. (ORPS Report ORO--MMES-X10CHEMTEC-1993-0005) Another event associated with the misuse of respiratory equipment occurred on July 18, 1991, at the Idaho National Engineering Laboratory Uranium Conversion/ Processing and Handling Facility. In this incident, a worker complained that his respirator was not filtering paint fumes properly. The follow-up investigation determined that the wrong filter canisters were used. Facility personnel determined that a lack of training resulted in the worker requesting the wrong type of respiratory filter canister. (ORPS Report ID--MKF-FPRCONST-1991-1011). These events emphasize the importance of respirator qualification training and the need for properly specifying, assembling, and inspecting respiratory equipment prior to use. DOE Order 5480.4, "Environmental Protection, Safety, and Health Protection Standards," mandates the requirements contained in American National Standards Institute Standard Z88.2, "Practices for Respiratory Protection," and 29 CFR 1910.134 for implementation of the Respiratory Protection Program and associated training of personnel. The DOE Radiological Control Manual provides additional guidance for implementation of a respiratory protection program. 3. PERSONNEL OVEREXPOSURE FROM MISHANDLING RADIOGRAPHY SOURCE On April 16, 1993, Scientific Inspection of Hixson, Tennessee, notified the Nuclear Regulatory Commission (NRC) that one of their employees received significant radiation exposure when he tried to manually adjust a stuck 99-curie iridium-92 radiography source. The calculated exposure to the individual's hand was 1,869 rem and the calculated whole body dose was 1.217 rem. The employee was taken to a hospital where his blood was tested and he was checked for contamination. The employee was taking industrial radiography pictures at a cogeneration plant in New Jersey when the source became stuck as he was cranking it out of the guide tube. The area had been roped off before beginning the radiography. Suspecting it was jammed, the employee approached the source with a radiation survey meter which went off-scale high. The meter is normally set on the 10X scale, which reads from 1 to 100 mrem/hour. He realized the source was out, returned to his crank station and tried to crank the source. However, the source would not move in either direction. The employee subsequently made three trips to the source attempting to free it, spending an estimated half-minute in the immediate area of the source with his hands about a half-inch from the source. After the third trip, he was able to crank the source back into its stored position. He then notified personnel at the job site what had happened and was transported to the hospital. (NRC Event Report No. 25409) There have been incidents involving problems with radiography equipment at DOE facilities. On February 4, 1992, a door limit switch failed on an X-ray generator being used for radiography at the Oak Ridge Y-12 Site causing the generator to be activated before the shielding door was fully closed (ORPS Report ORO--MMES-Y12QUALSER-1992- 0002). On February 14, 1991, radiography technicians at the Idaho Chemical Processing Plant experienced difficulty in retracting a radiography source after leaving the source guide tube bent at an angle and radius that did not allow the source to be freely retrieved into the shielded portion of the camera. Facility personnel identified the contributing cause and root cause as a less-than-adequate procedure and less- than-adequate training, respectively (ORPS Report ID--WINC-ICPP-1991-0030). There were no abnormal radiation exposures from either of these events. Descriptions of similar events in the commercial nuclear industry can be found in NRC Information Notice 91- 23, "Accidental Radiation Overexposures to Personnel Due To Industrial Radiography Accessory Equipment Malfunctions." Information Notice 91-49, "Enforcement of Safety Requirements for Radiographers," describes NRC mandated radiography safety requirements for NRC-licensed radiographers. Articles 365 and 665 of the DOE Radiation Control Manual (DOE/HT-0265T, June 1992) contain requirements applicable to conducting radiography at DOE facilities. Article 365 specifies the requirements related to operation and control of radiation generating devices and references the following documents: (1) DOE 5480.4, "Environmental Protection, Safety, and Health Protection Standards;" (2) "General Safety Standard for Installations Using Non-Medical X-Ray and Sealed Gamma-Ray Sources, Energies up to 10MeV;" (3) ANSI N43.2, "Radiation Safety for X-Ray Diffraction and Fluorescence Analysis Equipment;" and (4) 10CFR34, "Licenses for Radiography and Radiation Safety Requirements for Radiographic Operations." Article 655 specifies that "radiographers shall have training in accordance with 10 CFR 34.31. Radiation Generating Device Operators should have training comparable to that required by 10 CFR 34.31." DOE facilities involved in radiography or other operations of radiation generating devices should consider reviewing their facility compliance with the applicable sections of the DOE Radiological Control Manual. 4. REACTOR SCRAM WHILE PERFORMING ON-THE-JOB TRAINING On April 16, 1993, the Advanced Test Reactor (ATR) in Idaho automatically shutdown when an electrician conducting on-the-job training inadvertently tripped a 480-volt circuit breaker that supplied commercial power to components in three experimental test loops. Facility personnel initiated applicable emergency procedures, verified the cause of the scram, and ensured the reactor was in a safe shutdown condition. After verifying no problems with the circuit breaker existed, ATR operators restarted the reactor on April 18 following xenon decay. The electrician, instructing trainees on circuit breaker rack-in and rack-out procedures, received permission to operate on a spare 4160-volt breaker in the plant; he did so without incident. However, the instructor then decided to show the trainees, without actually operating circuit breakers, the differences in the rack-in/out procedures for different types of breakers. He did not notify operations personnel of his intent to do this. The instructor opened front panels for different types of breakers before reaching the subject circuit breaker. As he was pointing out a rackout latch mechanism, the instructor touched it with enough force to actuate it and cause the breaker to open but not rack out. (ORPS Report ID--EGG-ATR-1993-0015) During the event investigation, facility personnel determined that the electrician conducting the training knowingly violated Conduct of Operations guidelines and appropriate disciplinary actions are being considered. Investigators also identified weaknesses in the guidelines for conduct of on-the-job training by maintenance personnel in the plant and have suspended on-the-job training evolutions by those personnel until the guidelines are strengthened. Finally, a Test Reactor Area Safety Bulletin will be issued to communicate lessons learned from this event to facility personnel. In OE Weekly Summary 93-8, the Office of Nuclear Safety reported a similar event that occurred on February 18, 1993, at the Sequoyah commercial nuclear power plant where an electrical instructor caused a main turbine trip and a reactor scram while conducting on-the-job training. The instructor was using the main generator exciter field circuit breaker as an example to explain the operation of a certain type of circuit breaker. The plant was operating at 100 percent power at the time. The instructor received permission from the main control room to open the breaker cabinet door. After opening the door, he reached into the cabinet to point out a latching mechanism. As he was doing this, he inadvertently bumped the latching mechanism, tripped the breaker, and caused the turbine trip and reactor scram. (NRC Event Number 25101) These events demonstrate the importance of guidelines to control training activities on operating equipment. Permission should always be obtained for operations prior to entering energized panels or instrument panels. Control room and other supervisory personnel should carefully consider the potential consequences when granting permission to use operating equipment for on-the-job training. Guidelines related to control of training activities at DOE facilities may be found in DOE Order 5480.19, Conduct of Operations Requirements for DOE Facilities, Chapter V, Control of On-Shift Training." 5. GREASE SOLIDIFICATION CAUSES MOLDED CASE CIRCUIT BREAKER FAILURE On April 7, 1993, the Nuclear Regulatory Commission (NRC) issued Information Notice (IN) 93-26, "Grease Solidification Causes Molded Case Circuit Breaker Failure to Close," to inform commercial nuclear power plant licensees of a problem with a 400-amp frame, 600-Vac molded-case circuit breaker manufactured by General Electric Corporation (part number TJK436Y400). On March 26, 1992, a circuit breaker of this type failed to close while transferring electrical loads from an uninterruptible power supply (UPS) to the maintenance power supply at the Nine Mile Point Unit 2 commercial nuclear power plant. Failure of the breaker to close caused a loss of power to the standby gas treatment system radiation monitoring cabinet, a false high-radiation signal, a primary containment isolation, and the loss of a control room fire panel annunciator. Operators manually closed the circuit breaker and restored power to the affected equipment within approximately 12 minutes. Plant personnel determined that the breaker did not close because the grease used at the pivot points inside the breaker had dried out and solidified. When the grease dried out, it caused increasing friction and gouging at the metal-to-metal contact areas. This friction caused the breaker to become increasingly more difficult to close until finally the breaker would not close at all. Plant personnel located all breakers of the same make, model, and year as the failed one and scheduled their replacement. General Electric stated this type of molded case circuit breaker manufactured prior to 1985 used a soap-based or clay-based grease that could solidify with age, and they recommended field testing to identify such solidification. Since 1985, General Electric has replaced the soap-based and clay-based greases with synthetic grease that does not dry out and solidify with age. However, it is possible the older molded- case circuit breakers using the clay-based and soap-based grease may still be used at other facilities and could result in similar failures. Facilities utilizing General Electric molded case circuit breakers manufactured prior to 1985 should consider measures such as inspection, grease replacement, or breaker replacement. Preventative maintenance programs should include periodic inspection of electrical and mechanical component lubricant condition. 6. FRENCH EXECUTIVES ON TRIAL FOR NUCLEAR ACCIDENT On April 19, 1993, the former head of a French chemical company and two colleagues went on trial charged with causing actual bodily harm to three repairmen who suffered radiation poisoning in August 1991. The repairmen said they were not warned about a particle accelerator left on in a room where they worked. Untrained for working in a nuclear environment and unable to read instructions on the accelerator written in English, they were exposed in a few minutes to as much as 20 times the maximum radiation dosage considered safe for one year. All three repairmen suffered burns, hair loss, and skin irritation. All three individuals on trial face up to one year in prison if convicted. The incident is a reminder that personnel responsible for and involved in the operation of DOE facilities can, under certain circumstances, be held personally liable for actions that involve willful and deliberate violations of established regulations or law, particularly when such actions result in deaths, injuries, or other serious consequences. More importantly, it is an example of the need to enforce worker safety training requirements as mandated by Section 31.31(b) of the National Defense Authorizations Act for 1992 and 1993. 7. COOPER-BESSEMER DIESEL GENERATOR FUEL PUMP 10CFR21 NOTIFICATION On April 14, 1993, the Cooper-Bessemer Reciprocating Products Division of Cooper Industries sent the Nuclear Regulatory Commission (NRC) a 10CFR21 notification concerning defective fuel pumps in the "KSV" emergency standby diesel generator systems. The condition is significant since the defective fuel pumps may fail after only ten hours of operation. Cooper-Bessemer engineering personnel contend that the KSV emergency diesels can produce sufficient torque without one fuel injection pump (and therefore one cylinder out-of-service) to drive the attached electric generator and satisfy all plant design-basis electrical conditions. The defective fuel pump (part number 2-50F-049-001) was supplied to Cooper-Bessemer by the Haynes Corporation, Naples, Florida. The notification listed the Byron, Braidwood, Zion, Nine Mile Point, South Texas, Cooper, and Waterford commercial nuclear facilities as affected by the 10CFR21. The NRC event notification also stated that since November 1989, twelve pump failures have been reported at various facilities. The Cooper-Bessemer Owners Group that investigated these incidents attributed the cause of failure to the galling of the plunger and barrel in the fuel pump by silica and alumina particles. Most of these failures occurred within ten hours of the initial operation of the pump. The Owners Group determined the root cause to be a temporary breakdown of quality assurance requirements at the Haynes Corporation Naples facility during the manufacturing and rebuilding of the fuel pumps. (NRC Event Notification Number 25391) Cooper-Bessemer personnel reported that the breakdown in quality assurance requirements occurred during 1989 shortly after the fuel pump manufacturer moved operations from another location. They suspect that the alumina and silica contamination came from shot blast used to clean the pump hoses. Despite cleaning requirements, trace amounts of the abrasive material remained in the threaded areas of the fuel pump housing. As part of corrective actions, the fuel pump manufacturer has eliminated shot blast operations on the fuel pump housings and initiated an acid cleaning process. They also have initiated inspections prior to pump assembly to check for dirt or grit. Department of Energy facilities using diesels manufactured by Cooper-Bessemer should determine the applicability of the 10CFR21 notification and contact the vendor for further information. Cooper-Bessemer recommends that defective pumps be removed and returned to the manufacturer for rebuild. 8. UNABLE TO VERIFY CRITICALITY SAFETY-LIMIT COMPLIANCE On April 16, 1993, at the compact reactor fuel area of the uranium fuel fabrication facility in Lynchburg, VA, Babcock & Wilcox personnel notified the Nuclear Regulatory Commission when they determined that compliance with a nuclear criticality safety limit could not be shown because of inability to demonstrate compliance with a posted administrative limit on concentration of uranium-235. This condition was discovered during a practice run for a new process. A placard in bay 13A in the fuel washing station of the compact reactor fuel area required operators to limit uranium- 235 concentrations to 1,500 grams per liter of highly enriched uranium. While a majority of the uranium handled in bay 13A for the last two to three years was depleted, some was highly enriched. The posting was active during this time. A criticality safety evaluation for the posted area relied on two barriers: the posting, and minimum spacing of fuel washing cans. The safety evaluation, prepared by the nuclear criticality safety group, specified the posting limit and it was reviewed and approved by affected operations and engineering groups. Facility personnel reported that can spacing was maintained by passive, geometric-type, engineering controls. Personnel also reported that fuel-washing operations make certain physical changes to the fuel. This meant it was impossible for the bay 13A operators to verify compliance with the posting. The placard stated, in part: "If this limit cannot be met, notify Nuclear Criticality Safety." No such notifications were recorded. Also, according to facility personnel, applicable operating procedures stated that if any step in the procedure could not be met, then the operator must stop work and notify the supervisor. The facility has been shut down until an evaluation is performed to determine correct, verifiable wording on the sign. (NRC Event Number 25405) For Department of Energy facility contractors, DOE Order 5480.24, "Nuclear Criticality Safety," provides direction on establishing nuclear criticality safety program requirements. This order establishes a double contingency principle to prevent a criticality accident and provides necessary elements for criticality safety programs. Also, the order invokes several American Nuclear Society Standards for basic elements and control parameters of programs for nuclear criticality safety. DOE Order 5480.19, "Conduct for Operations Requirements for DOE Facilities," provides necessary elements for operator aid postings. As stated on pages I-95 and I-96, a program should be established to ensure that postings "...are current, correct, and useful," and that postings "...should be reviewed periodically to ensure they are still correct and necessary." This event also demonstrates the need for a questioning attitude on the workers' part. Workers should routinely ask themselves if an instruction, such as a posting, is understandable and achievable, and, when in doubt, ask supervision for clarification or direction before proceeding. Also, a training needs analysis of procedures and operator aids that identify necessary worker skills, knowledge, and abilities can be helpful in finding unclear and erroneous instructions. 9. LEVEL INSTRUMENTATION INACCURACIES OBSERVED DURING NORMAL PLANT DEPRESSURIZATIONS On April 8, 1993, the Nuclear Regulatory Commission issued Information Notice 93- 27, "Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization." The Information Notice describes an event at a commercial nuclear power plant and provides background information on inaccuracies in reactor-vessel level indication and how these errors could result in complicated long-term operator actions and possible loss of automatic actuation of safety systems while the reactor is in a reduced-pressure condition. On January 21, 1993, during a plant cooldown following a reactor scram at Washington Nuclear Power Plant Unit 2, "notching" of the level indication was observed on at least two of four channels of the reactor-vessel narrow-range level instrumentation. ("Notching" is a momentary increase in indicated water level.) This increase occurred when a gas bubble moved through a vertical portion of the reference leg and caused a temporary decrease in the static head in the reference leg. The notching was first observed on one channel at a pressure of approximately 120 psig and on another starting at approximately 50 psig. At these pressures, the level error was in the approximate range of 4 to 7 inches. Beginning at a pressure of about 35 psig, level indication from one channel became erratic and, as the plant continued to depressurize, a 32-inch error occurred. The 32-inch level error was sustained and gradually recovered over a period of two hours. The licensee postulated this large error in level indication was caused by gas released into the reference leg displacing about 40 percent of the water volume. The licensee also postulated that the slow recovery of correct level indication resulted from the time needed for steam to condense in the condensate chamber and refill the reference leg. The licensee inspected the reference leg for the channel with the 32-inch level error and discovered leakage through reference leg fittings. This could have been a contributing factor to accumulation of dissolved noncondensible gas in that reference leg. The licensee determined that the false high level indication observed could result in a failure to automatically isolate a leak in the residual heat removal system during shutdown cooling. The design basis for the unit included a postulated leak in the residual heat removal system piping outside containment during shutdown cooling. The licensee implemented compensatory measures for future plant cooldowns to ensure that a leak could be promptly isolated. The Nuclear Regulatory Commission previously issued Information Notice 92-54, "Level Instrumentation Inaccuracies Caused by Rapid Depressurizations," and Generic Letter 92-04, "Resolution of the Issues Related to Reactor Vessel Water Level Instrumentation in BWRs Pursuant to 10 CFR 50.54(f)," to discuss how noncondensible gas may become dissolved in the reference leg of water level instrumentation and lead to false indications of high level after a rapid depressurization event. These events underscore the importance of considering all factors that could affect proper instrument operation. Unaccounted-for fluid transients could prevent proper instrument operation and thereby prevent or degrade safety-related equipment operation. 10. OPERATOR INCORRECTLY STARTS WRONG EMERGENCY DIESEL GENERATOR On April 20, 1993, an operator at the Quad Cities commercial nuclear power facility incorrectly started the wrong diesel generator, causing an inadvertent operation of an emergency safety system. The operator started the unit 1 diesel instead of the unit 1/2 swing diesel as part of an output breaker test. The unit 1 diesel started, but did not load. Upon discovery, facility personnel secured the swing diesel. Reactor operations were not affected by this event, and there was no damage to the swing diesel or other plant equipment. The control switches for the unit 1 emergency diesel and the swing diesel are located on the same panel approximately 20-inches apart, with the unit 1 diesel operating switch painted black and the swing diesel painted orange. The operator was directed to start the swing diesel and load it to unit 2 to test the operation of the output breaker. The operator had reviewed and walked through the procedure, looking at the panel indications. Another operator was sent to confirm the readiness of the swing diesel prior to beginning the test. After receiving confirmation that the swing diesel was ready, the operator made an announcement over the plant page system that the swing diesel was being started. He then walked over to the panel and turned the switch for the unit 1 diesel instead of the swing diesel. (NRC Event Notification Number 25417) Personnel errors are a significant contributor to many events at Department of Energy facilities and at commercial nuclear power plants. The Office of Nuclear Safety reported other occurrences involving personnel error and self checking in Operating Experience Weekly Summaries 92-17, 92-19, 92-24, 92-33, and 93-08. As previously reported, the commercial industry, with guidance from the Institute for Nuclear Power Operations, is addressing the problem with a program called Self-Checking. This technique is described in Good Practice OE-908, Self Checking. Self Checking is a risk management tool designed to reduce the potential for human error by helping facility personnel focus their attention on the details of the task at hand. This event emphasizes the importance of self-checking to reduce human error. This event may not have occurred if the operator had focused on the proper switch to activate. Self Checking techniques are used widely at commercial nuclear power plants to prevent human performance problems and can identify a potential human performance error before it occurs. The Institute of Nuclear Power Operations also recently issued Significant Operating Experience Report 92-1, Reducing the Occurrence of Plant Events Through Improved Human Performance. This document describes lessons learned by member commercial utilities in addressing the principal causes of human performance problems, and also describes essential elements identified from a review of several successful commercial utility programs to address human performance problems. ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES 1. WORKER CONTAMINATIONS DURING CONSTRUCTION ACTIVITIES In OE Weekly Summary 93-1, the Office of Nuclear Safety reported a contamination event that occurred on December 29, 1992, at the Bethel Valley Liquid Low-Level Waste (BVLLW) Upgrade Project at Oak Ridge National Laboratory. Nineteen workers were contaminated and low-level contamination from the event was spread to surrounding grade-level areas. At the time, the cause of the contaminations was attributed to a leaking pipe. (ORPS Report ORO--MKFO-X10CENTENG-1992-0026) Site personnel have since completed a Type B investigation of the event and issued report DOE/OR-1082, "Type B Investigation of the Contamination Accident at the BVLLW Upgrade Project." According to the report, the workers were contaminated while performing construction activities at a new but not yet operating radioactive waste-collection facility. Waste drains from an operating radioanalytical laboratory had been connected to the new waste receiving facility in early December. Radioactive waste was inappropriately introduced into the new but not yet authorized laboratory drain system, and water was later released into the construction site during installation of valve instrumentation in the drain line. Additionally, a mixture of rainwater and contaminated liquid was pumped to a nearby grade-level area which was subsequently surveyed and posted as a contamination area. Surveys confirmed that no contamination reached the storm drain. The Monitoring and Control Station (MCS), which is a part of the BVLLW Upgrade Project, is intended to receive low-level radioactive waste from the Radioactive Materials Analytical Laboratory (RMAL) in Building 2026. Workers came in contact with radioactive liquid in the MCS tank and valve vault areas while performing various construction activities. The liquid exited through taped-over piping when a valve was cycled several times. The workers noticed the liquid but assumed it was rainwater or condensate. One worker removed the tape thinking the liquid would empty out; however, a continuous trickle was observed, and the tape was placed back in position. The workers were not aware of their contamination until the end of the work shift when employee comments regarding the liquid coming from the cut pipe were overheard by a fellow employee. The employee was aware that Building 2026 handled radioactive materials and that the MCS was tied into Building 2026. After confirming that the workers had contacted the liquid, he contacted supervision to initiate worker contamination surveys. Several workers were found to be contaminated and efforts were initiated to recall potentially contaminated workers who had already left the site. The Investigation Board used the Management Oversight and Risk Tree (MORT) method and Barrier Analysis to investigate the event. According to the report, the direct cause was introduction of liquid low-level radioactive waste into the new drain system in Building 2026, Laboratory 100, which leads to the MCS where construction personnel were working. The new drain system was not ready for authorized use. The Board identified 13 contributing causes in the areas of Risk Assessment, Job Safety Analysis, Conduct of Operations, and Management and Oversight. Finally, the Board concluded there were three root causes: (1) a failure to identify the hazards and properly analyze job safety, (2) a failure to apply Conduct of Operations principles related to personnel protection, and (3) a failure to provide proper safety oversight. The report provided 16 specific recommended measures to prevent recurrence of a similar event. In general, the Board recommended that management review their health and safety programs to ensure a safe working environment for employees involved in concurrent operations and construction activities, and that the review be an integral part of every phase of a construction project, from initial planning through operation. The report further recommended that risk assessment of tie-ins to operating areas be performed to understand and respond to potential vulnerabilities. Other recommendations, including one for a special emphasis on Conduct of Operations during concurrent construction and operations activities, were made in the report. SAFETY NOTICES UNDER DEVELOPMENT Note: The Office of Nuclear Safety encourages input related to the development of Safety Notices. If you have any questions, comments, or information concerning events or issues similar to the following, please contact Ivon Fergus, Office of Nuclear Safety at (301) 903-6364. 1. NS has identified a number of events related to the loss of annunciators and other safety-related equipment because of problems involving 120-VAC/125- VDC systems at DOE and commercial facilities. NS is reviewing potential generic problems associated with the adequacy of 120-VAC/125-VDC systems at DOE facilities. 2. NS evaluated three events associated with the temporary diesel generator at the Rocky Flats Plant, Building 707. The lessons learned from these events, particularly as they relate to the control of temporary modifications, are being considered for dissemination in an NS Safety Notice. 3. NS is developing a Safety Notice concerning problems with Uninterruptible Power Supplies (UPS). 4. NS is considering development of a Safety Notice related to control of work at electrical substations and switchyards. 5. NS is working with Lawrence Livermore National Laboratory and DOE-SF personnel to develop a Safety Notice on cracking in ventilation ducting. 6. NS is considering developing a Safety Notice related to fuel oil supplies for Emergency Diesel Generators (EDGs). 7. NS is developing a Safety Notice to address uses of independent verification for equipment positioning. 8. NS is developing a Safety Notice in regards to maintaining important alarm and monitoring systems at facilities undergoing Transition and Decontamination & Decommissioning. SAFETY NOTICES PREVIOUSLY ISSUED Safety Notice No. 91-1, "Criticality Safety Moderator Hazards," September 1991 Safety Notice No. 92-1, "Criticality Safety Hazards Associated With Large Vessels," February 1992 Safety Notice No. 92-2, "Radiation Streaming at Hot Cells," August 1992 Safety Notice No. 92-3, "Explosion Hazards of Uranium-Zirconium Alloys," August 1992 Safety Notice No. 92-4, "Facility Logs and Records," September 1992 Safety Notice No. 92-5, "Discharge of Fire Water Into a Critical Mass Lab," October 1992 Safety Notice No. 92-6, "Estimated Critical Positions (ECPs)," November 1992 Safety Notice No. 93-1, "Fire, Explosion, and High-Pressure Hazards Associated with Drums and Containers," February 1993 Copies of NS Safety Notices may be requested from: Nuclear Safety Information Center, Office of Nuclear Safety, U.S. Department of Energy, Room S161, GTN, Washington, DC 20585