OPERATING EXPERIENCE WEEKLY SUMMARY 93-38 September 17 through 23, 1993 The purpose of the Office of Nuclear Safety (NS) Operating Experience (OE) Weekly Summary is to enhance safety throughout the Department of Energy (DOE) complex by promoting feedback of operating experience and encouraging the exchange of information among DOE nuclear facilities. The OE Weekly Summary is distributed for information only. No specific actions or responses are required solely as a result of this document. Readers are cautioned that review of the OE Weekly Summary should not be relied upon as a substitute for a thorough review of the interim and final Occurrence Reports. The following events were reviewed during the week of September 17 through 23, 1993. ITEM PAGE 1. FOREIGN MATERIAL FOUND IN REACTOR VESSEL 2 2. VIOLATION OF TECHNICAL STANDARD AT CPP-603 FACILITY 3 3. SWITCHES FOUND IN IMPROPER POSITION 4 4. CRITICALITY CONTROL VIOLATION AT BABCOCK AND WILCOX FACILITY 5 5. INCORRECT USE OF CHAIN AND HASP LOCKOUT 6 6. INADVERTENT BREAKER OPERATION CAUSES POWER OUTAGE TO MULTIPLE FACILITIES 7 7. EMPLOYEE DRIVES METAL FENCE POST INTO 480-VOLT BURIED CABLE 8 8. INTENTIONAL DEGRADATION OF NUCLEAR INCIDENT MONITOR ALARM 9 9. WORKER BURNED FROM ENERGIZED WIRE 10 ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES 1. IDAHO TEST REACTOR AREA HOT CELL RADIATION STREAMING EVENT CORRECTIVE ACTIONS 11 1. FOREIGN MATERIAL FOUND IN REACTOR VESSEL On September 15, 1993, personnel at the Advanced Test Reactor in Idaho submitted an off-normal occurrence report after discovering foreign material in the reactor vessel for the second time in less than a week. On September 8, facility personnel found a damaged C-cell battery in the vessel and then found crushed flashlight parts on September 13. All foreign material was located outside the core region and there was no fuel damage. After removing the C-cell battery on September 8, facility personnel performed a thorough examination of the vessel and found no other debris. Although engineers could not determine how the battery got into the vessel, facility management concluded it was unlikely that there was other debris in the vessel. Site personnel reported that a certain amount of foreign material in the vessel is analyzed for and determined to be acceptable in the facility Safety Analysis Report. Facility personnel closed up the vessel and conducted operational tests at approximately four megawatts for 20 minutes. The vessel was then reopened, new flux monitors installed, another internal inspection performed, and a similar operational test conducted. Workers found the crushed flashlight parts during a subsequent vessel inspection on September 13. (ORPS Report ID--EGG-ATR-1993- 0032) Management personnel placed a hold on reactor operations and initiated efforts to locate the remaining flashlight parts and to determine the entry point of the flashlight into the primary coolant system. After conducting various activities designed to retrieve the remaining parts and finding some small pieces, facility personnel located a white plastic ring floating beneath a screen on the inlet side of the reactor. Site personnel reported that the location of the ring indicated the flashlight most likely entered the primary coolant system at a point other than the reactor vessel. Facility personnel reviewed work performed during the previous outage and determined that the flashlight probably entered the system through the outlet piping of a primary coolant emergency pump during maintenance. Facility personnel reviewed the Safety Analysis Report and determined that the remaining amount of material in the vessel, assuming an entire flashlight entered the system, would not adversely impact safe operation of the reactor. However, personnel continued efforts to remove additional foreign material. Site personnel planned to conduct an evaluation of foreign material exclusion (FME) practices and procedures in place when the flashlight entered the system. Preliminary indications are that FME controls may not be as formal during work on systems connected to the reactor vessel as they are during work around the vessel when it is open. This event underscores the need for effective FME procedures and controls to protect critical equipment and systems at DOE facilities from degradation caused by foreign material. Facility personnel should be aware of the potential for foreign material migration to critical equipment from systems and equipment that, without a thorough technical evaluation, may not seem to present such a potential. DOE 4330.4A, Maintenance Management Program, Section 8.3.3, states that maintenance supervisors should routinely monitor work in progress and check for good work practices, including "open system and component protection." 2. VIOLATION OF TECHNICAL STANDARD AT CPP-603 FACILITY On September 19, 1993, operations personnel at the Idaho National Engineering Laboratory CPP-603 Irradiated Fissile Materials Storage facility discovered two fuel-laden carbon-steel hangers, or yokes, improperly spaced and in violation of the technical standard designed to provide criticality safety. Although the technical standard was violated, there was no criticality concern because the fuel was not highly reactive and the distance between the fuel buckets was greater than the edge-to-edge requirement that prevents neutron interaction in water. (ORPS Reports ID--WINC-FUELRCSTR-1993-0009) Building CPP-603 is a facility used for underwater storage of nuclear fuel in three underwater storage basins (north, south, and middle) and above-ground dry storage. Irradiated fuel is suspended from a monorail system by single elements or in buckets which can contain several small elements. The elements or buckets are attached to hooks, generally made of stainless steel, that are welded to a steel yoke (carbon or stainless) hanging from the monorail. The yokes have upper and lower bumpers to ensure that correct spacing and adequate separation are maintained for criticality safety, and they are classified as an engineering safety feature. The facility Technical Standard states that the north and middle storage basins will be inspected quarterly to ensure that like yokes are segregated into rows and that unlike yokes in the same row are separated by an empty yoke and bucket to provide blank spacing. The facility safety analysis report requires a water space of eight inches (edge- to-edge) between fissile materials to provide near neutron isolation from neutron interaction in water. This spacing is provided by the yoke-bumper design for like yokes, which are dimensionally identical. Unlike yokes have different spacing from the trolley to the lower bumpers, and the bumpers will be mismatched. Mismatched bumpers do not prevent adjacent yokes from approaching closer than eight inches. Facility personnel avoid this problem by placing only like yokes in a row. However, if unlike yokes are in the same row, workers separate them by placing an empty yoke and bucket between them, thus ensuring neutronic isolation. Workers recently moved the subject yokes during performance of Special Procedure #220-93 "SNAP Fuel Re-spacing, Rerigging, and Re-storage." Two operators visually verified the yokes as like yokes by looking through approximately 22 feet of water to determine if the bumpers were five feet apart and of equal height from the monorail. During the bi-monthly inspection, facility personnel actually measured the height of the yokes and discovered a six inch difference between them, which verified the yokes to be unlike. Upon discovering this, the workers reverified the measurements and notified management. Facility personnel reported that the special procedure that had been used did not provide objective criteria for inspecting the bumpers and did not require use of measurement devices. In this event, the two yokes were separated by an empty yoke without the required bucket. Facility personnel reported that the edge-to-edge distance was approximately 30 inches, well above the eight-inch edge-to-edge requirement; and the fuel in the buckets was not highly reactive. The criticality safety criteria section of the Plant Safety Document (the Safety Analysis Report) for building CPP-603 established criticality prevention measures and described two conditions that could lead to a criticality event. The first was a failure to properly isolate highly reactive fuel handling units (FHU) suspended from the monorail system. The second was the release of an FHU from its intended monorail storage position. NS reported in OE Weekly Summary 92-22 about the loss of these barriers at CPP-603. On September 18, 1992, an engineering team determined that 25 highly reactive FHUs were in adjacent positions without proper spacing. This was significant because a criticality event could result if these elements dropped to the basin floor and achieved an unfavorable geometry, thus violating the first condition described in the Plant Safety Document. Prior to that event on March 16, 1992, a corrosion engineer discovered that one of the FHU yokes failed because of corrosion. This yoke was not used for storage of nuclear fuel elements at the time of the failure. Facility personnel subsequently declared that the corroding carbon steel yokes resulted in an unreviewed safety question, constituting an occurrence of the second condition described in the Plant Safety Document (ORPS Report ID--WINC-ICPP-1992-0024). Facility personnel developed Special Procedure #220-93 because of these criticality concerns. Corrosion of fuel storage equipment continues to be a problem at CPP-603. NS reported in OE Weekly Summary 93-37 about recent fuel corrosion problems at the facility. On September 13, 1993, personnel were rigging a fuel handling bucket containing a canister of System for Nuclear Auxiliary Power fuel in preparation for re-storage when the canister broke apart because of corrosion. Approximately 14 inches of the top section of the canister and three fragments of highly reactive fuel pins separated and fell onto the safety catch pan located under the storage bucket. (ORPS Report ID--WINC-FUELRCSTR-1993-0007) 3. SWITCHES FOUND IN IMPROPER POSITION On September 14, 1993, operations personnel at Rocky Flats Building 779 discovered the Hand-Off-Auto-off (HOA) switches for standby exhaust fans F401A and F402A in an improper position. These fans are part of the glovebox and hood exhaust system. The Stationary Operating Engineer (SOE) identified the improper switch configuration prior to performance of the monthly fan rotation surveillance procedure. Earlier in the day, the facility maintenance electricians and systems engineer performed a Post-Maintenance Test on these fans and the test procedure required the HOA switch to be placed in the OFF position and verification that the backdraft dampers were open. Facility personnel completed this task and the SOE returned the switch to the AUTO position. The SOE verified this action by radio contact to operators in the utilities control room. During the next shift, control room operators preparing to perform the surveillance test noticed a motor stop light for the fans, indicating that the switches were in the OFF position. Both the utilities manager and the SOE confirmed that the HOA switches for both fans were in the OFF position. The utilities manager returned the HOA switches to the AUTO position and notified the shift manager of the event. Facility personnel subsequently successfully completed the surveillance of the fans. Facility personnel are investigating the event for identification of corrective actions and lessons learned. They attributed the direct cause of this occurrence to inattention to detail (i.e., personnel failing to maintain the HOA switches in the proper position). DOE and internal security were notified of this event. (ORPS Report RFO--EGGR-ANALYTOPS-1993- 0139) On August 16, 1993, a similar event occurred at the facility during the monthly fan rotation surveillance. In this incident, the Building 559/779 utilities manager discovered the HOA switch for Building 779 exhaust fans F401A/B was not in the AUTO position as required. The improper switch position resulted in no standby fan capability. The SOEs attempted the monthly fan rotation and exhaust fan F401B did not activate as required. The utilities manager proceeded to check the HOA switch and discovered the improper position. On August 13, 1993, facility personnel performed a loop calibration on this fan. However, they reported that all information (i.e., visual confirmation and work package signatures) indicated the switch was placed in the AUTO position as required. There was no activity on this system between the loop calibration and the discovery. Facility personnel are still investigating the cause of how the switch was placed in the wrong position. (ORPS Report RFO--EGGR-ANALYTOPS-1993-0118) These events emphasize the importance of maintaining system configuration by performing lineups after maintenance and before returning systems and components to service, including independent verification of procedure sign-offs as applicable. Switches or valves left out of their normal positions should be tagged or otherwise marked to avoid operational problems resulting from operators assuming that they are in the normal position. Information on other equipment mispositioning events can be found in Institute for Nuclear Power Operations (INPO) Significant Event Report 6-92, "Valve Mispositioning Events," INPO Significant Operating Experience Report 85-2, "Valve Mispositioning Events Involving Human Error," and Nuclear Regulatory Commission Information Notice 87-25, "Human Error - Wrong Unit, Train, or Component." 4. CRITICALITY CONTROL VIOLATION AT BABCOCK AND WILCOX FACILITY On September 16, 1993, personnel at the Babcock and Wilcox (B&W) Uranium Fuel Fabrication facility in Lynchburg, Virginia, discovered a violation of an administrative criticality control and reported the event in accordance with Nuclear Regulatory Commission (NRC) Bulletin 91-01. They discovered 436 grams of uranium-235 in a room where the maximum mass limit was 350 grams. Workers were chemically separating organic, aqueous, and carbon tetrachloride mixed wastes containing highly enriched uranium oxycarbide when the event occurred. When solutions of uranium-235 are taken into the processing laboratory, facility personnel are required to log the mass content to ensure that the total does not exceed 350 grams. In this event, workers brought a drum into the work area that contained two different solutions with separate mass values for each solution. The records accompanying the drum indicated the proper values. When they recorded the mass value in the laboratory log, only one of the two values was entered. When the accounting discrepancy was discovered later in the day, workers immediately removed the material from the area. Facility personnel reported that, although the mass amount exceeded administrative limits, the quantity was below the actual critical mass amount of 820 grams. In addition, the second criticality contingency of a minimum required spacing between containers was never violated. Facility personnel are investigating the event for identification of corrective actions and lessons learned. NRC Bulletin 91-01, "Reporting Loss of Criticality Safety Controls," requires all fuel cycle and uranium fuel research and development licensees to report violations of criticality contingencies. (NRC Event Notification Number 26099) For DOE facility contractors, DOE 5480.24, "Nuclear Criticality Safety," provides direction on establishing nuclear criticality safety program requirements. This order establishes a double contingency principle to prevent a criticality accident and provides necessary elements for criticality safety programs. Also, the order invokes several American Nuclear Society Standards for basic elements and control parameters of programs for nuclear criticality safety. 5. INCORRECT USE OF CHAIN AND HASP LOCKOUT On September 14, 1993, a locked-out fan pulley at the Savannah River K-Reactor began to rotate slowly while maintenance personnel were replacing the belts on the fan. The fan rotation was caused by differential pressure from an operating fan sharing the same suction and exhaust header, a phenomena referred to as windmilling. The inability of the lockout to prevent the fan pulley from rotating raised concerns regarding the adequacy of the lockout and the potential for personnel injuries when operating equipment locked out in a similar manner. There were no personnel injuries or equipment damage caused by the event. The lockout, installed to allow replacement of the fan belts, isolated electrical power to the motor and included a chain wrapped through the spokes of the pulley and around a bearing pedestal and locked with a hasp to prevent rotation caused by windmilling. After mechanics removed about half of the belts from the fan, the hasp and chain came loose and the fan pulley began to rotate slowly. Investigators determined that the hasp, normally used to prevent personnel from inadvertently operating equipment, not as a load-bearing blocking device, was not capable of withstanding the stress caused by the windmilling and failed. Initially, the friction from the belts connected to the motor was sufficient to prevent windmilling. However, as the mechanics removed the fan belts, friction was reduced until the windmilling force was sufficient to cause rotation of the pulley and failure of the hasp. Facility personnel also noted that the suction damper for the fan, which helps minimize the windmilling effect when closed, was not included in the lockout. Facility personnel stopped all work on the fan and other equipment using similar lockouts while the event was investigated. Investigators found that one part of the Reactor Division safety manual specified using a chain and lock while another part of the manual stated that a timber (such as a 4X4) should be used as a blocking device. Workers had not been using timbers because they caused difficulties in removing the belts and because of the conflicting safety manual requirements. Facility personnel are developing a locking device that will allow unrestricted removal of the fan belts and at the same time provide enough strength to absorb the windmilling forces. (ORPS Report SR--WSRC-REACK- 1993-0156) This event underscores the need for personnel at DOE facilities to ensure that devices used to restrain equipment from operating are designed to withstand the resulting stresses. Failure to do so, especially when personnel are working near the restrained equipment, could result in serious personnel injury or damage to nuclear safety-related equipment. In this incident, the hasp was used to restrain the fan from rotating and failed because it was not designed to withstand the resulting stresses. Also, site safety manuals should specifically address use of lockouts designed to physically prevent equipment movement, as opposed to preventing human operation. 6. INADVERTENT BREAKER OPERATION CAUSES POWER OUTAGE TO MULTIPLE FACILITIES On September 20, 1993, an operator performing preventive maintenance at a substation at the Savannah River Site opened the wrong circuit breaker, causing a loss of power to multiple facilities, including the Effluent Treatment Facility (ETF), the H-Area Tank Farm, and administrative facilities. The ETF processes slightly radioactive water for release to the environment, and the H-Area Tank Farm is a high-level radioactive liquid waste storage facility. Backup diesel generators at both facilities started and operated as designed. There was no adverse impact to personnel safety or the environment as a result of the event. (ORPS Reports SR--WSRC-POD-1993-0032, SR--WSRC-ETF-1993-0007, SR--WSRC- HTANK-1993-0066) Facility personnel indicated the power outages were caused by personnel error when an electrical equipment operator working in a switchyard inadvertently opened a 13.8kv feeder breaker. The operator set his work package down behind him and turned around to operate a permissive switch to allow opening of a cubicle for a just-opened breaker. However, he turned the switch on the breaker next to the correct one instead. Site personnel reported the breakers were adequately labeled and the operator had an approved work package and procedure plus 15 years experience at the site. The power outages lasted for approximately one hour. All power was lost to the ETF and the Old Hill Tank Farm (part of the H-Area Tank Farm). The ETF was operating under normal conditions when power was lost and operators verified that emergency generators were operating and ensured the plant was in a safe shutdown condition. The Old Hill Tank Farm evaporator was not operating at the time. However, power was lost to storage tank ventilation purge fans. Operators verified operation of emergency generators and restarted the fans. Although there were no serious consequences from this event, it underscores the need for extra precautions and awareness when operating equipment that, if improperly operated, could adversely impact operations at multiple facilities. NS described events caused by personnel errors in previous OE Weekly Summaries and referred to a technique referred to as self-checking. Self-checking is a risk management tool designed to reduce potential for human error by helping facility personnel focus attention on details of the task at hand and to identify and avoid potential human errors before they occur. This technique is widely used in the commercial nuclear industry, and the Institute for Nuclear Power Operations (INPO) has issued a number of documents describing the elements of effective human error reduction programs at commercial nuclear utilities. Also, many commercial nuclear utilities incorporate two-man switches at high voltages to prevent errors and protect personnel. 7. EMPLOYEE DRIVES METAL FENCE POST INTO 480-VOLT BURIED CABLE On September 16, 1993, personnel at the Idaho Chemical Processing Plant discovered that the overhead crane in the Fuel Process Restoration (FPR) facility would not function because of a loss of power. Personnel investigated the event and discovered that a fence post had severed the 480-volt buried cable supplying temporary power to the crane. On August 30, 1993, workers installed four fence posts in the ground as anchors for a trailer and a housing that supported a soil sample drilling project. After cutting the cable, the workers did not immediately notice the loss of power because the FPR crane was not in use. Facility personnel discovered the condition when they attempted to switch the power feed to the crane from temporary to permanent. As part of the soil sample drilling project, facility personnel obtained an excavation permit that detailed the locations of telephone cables, imbedded electrical cable, and underground piping. The temporary buried cable for the FPR crane was documented on the permit. The workers installing the fence posts apparently did not properly check the permit prior to driving the posts. In addition, the cable was buried only two feet deep and was not identified by marker flags (ORPS Report ID--MKF-MKNE-1993-0001). A similar event occurred on September 15, 1993, at the Savannah River Effluent Treatment Facility when a worker encountered an underground pipe while drilling for a soil sample. The pipe was a low-level radioactive waste-water transfer line made of high- density polyethylene. The jacketed portion of the pipe was damaged, but facility personnel reported that no waste water was released to the public. Facility personnel conducted a critique and determined that the causes included lack of preparation of an evacuation permit, relocation of the drilling stakes approximately 20 feet south of their originally surveyed location without proper followup, and lack of established work control procedures. In December 1992, workers surveyed and staked the area where the drilling was planned. Six months later they conducted a ground penetrating radar survey of the area to identify underground interferences. In July 1993, workers moved to a new drilling location in order to clear the overhead power line right-of-way. This new location was outside the originally surveyed boundary. The workers failed to perform either a ground- penetrating radar or a coordinate survey at the new stake locations (SR--WSRC-ETF-1993- 0005). NS discussed problems with damage to underground cable, piping, conduits, and structures during excavations in previous OE Weekly Summaries. Several events in this category could have resulted in serious personnel injury. On September 14, 1992, an underground natural gas pipeline ruptured when it was struck by a back hoe during an electrical utility relocation project at the Lawrence Berkeley Laboratory. Facility personnel previously surveyed the area for underground obstructions in accordance with procedures, but a change in the job order altered locations. The workers failed to survey the new area and subsequently punctured an underground gas line with a back hoe. No one was injured as a result of this event (ORPS Report SAN--LBL-OPERATIONS-1992-0007). A follow-up investigation determined that facility drawings were not adequately updated to show the location of the gas line when it was installed in 1989. There was no tape or trace wire installed marking the location of the line. In addition, facility personnel reported that the pipeline was buried closer to the surface than required by code (OE Weekly Summary 92-21). A similar event occurred on October 10, 1991, when personnel at the Los Alamos National Laboratory ruptured an underground natural gas line with a back hoe. They obtained an approved evacuation permit and all utilities were properly marked for location. However, the depth of the piping could not be properly measured with instruments available and facility personnel failed to follow procedures that required manual exploration prior to machine excavation. The piping was buried only 10 to 12 inches below the surface (ORPS Final Report ALO-LA-LANL-PHYSTECH-1991-1009). Another near miss occurred on September 20, 1991, at the Grand Junction Operations facility when a worker severed a 13,000 volt underground power cable located one foot below the surface while removing mill tailings at the Uranium Mill Tailings Remedial Action Site. Facility drawings incorrectly showed the cable as being buried four feet deep and encased in concrete (ORPS Report ID--GEO-GJO-1991-1019). These events demonstrate the necessity to thoroughly investigate the possibility of underground obstructions prior to commencing excavations. Review of plant facility drawings may not be adequate for locating potential underground cables, conduits, tanks, or piping. In addition, facility record drawings may lack information necessary to assure correct marking of buried utilities. Excavations around utilities should be dug using hand tools. Security and telecommunication personnel should be consulted prior to digging to assist in identification of buried components. Facility procedures controlling excavations should provide detailed steps for locating underground obstructions. Likewise, underground cables, including temporary installations, should be identified with locator flags. At commercial nuclear power plants, personnel often use cable locating equipment such as Dynatel manufactured by the 3-M Corporation or ground-penetrating radar to locate cables prior to excavation. 8. INTENTIONAL DEGRADATION OF NUCLEAR INCIDENT MONITOR ALARM On September 20, 1993, a supervisor performing daily checks of a Nuclear Incident Monitor (NIM) test panel at the Savannah River Reactor Materials facility discovered that an alarm on the panel had been intentionally muffled. The alarm, which had been taped over, functions to warn operators if electronic circuitry detects a functional problem with any of the building NIMs. There was minimal impact on the ability to warn site personnel of an actual nuclear incident because (1) the taped alarm was not needed for that purpose and (2) a redundant NIM for each monitored area is available in the event a problem with one NIM is undetected because of the taped alarm. Investigators determined that the alarm was taped over sometime between Thursday morning (16 September) and Monday morning (20 September) when it was discovered. Facility personnel have not determined who taped over the alarm or why, but suspect the alarm may have sounded during an electrical storm and 40-minute power outage on Friday evening. Workers removed the tape from the alarm and retested it for proper audio response. Planned corrective actions include revision of the daily NIM check procedure to specifically require inspection of the alarm for obstructions and reemphasizing to facility personnel the importance of not tampering with alarms and warning systems. (ORPS Report SR--WSRC-RMAT-1993-0017) In OE Weekly Summary 92-21, NS reported other events involving intentional disabling and misuse of alarms and warning systems at DOE facilities. On September 13, 1992, Rocky Flats personnel discovered that some workers changed the radio frequency on a Life Safety/Disaster Warning (LS/DW) system radio transmitter and used the headsets to listen to music (ORPS Report RFO--EGGR-PUFAB-1992-0254). On January 7 and 20, 1992, personnel discovered a pair of orange visitor coveralls taped around the inner cone of a LS/DW speaker and T-shirts stuffed into another speaker at Rocky Flats (ORPS Report RFO-- EGGR-PUFAB-1992-0008,0013). On November 27, 1991, Argonne National Laboratory - West personnel discovered that the volume on a Life Safety System speaker had been turned so low as to effectively turn it off. Investigators determined that the root cause of the event was the failure of management to effectively communicate the hazards associated with adjusting the volume on speakers intended to support life safety functions. (ORPS Report CH-AA-ANLW-FCF-1991-1006) These events illustrate that all personnel at DOE facilities may not fully understand the safety significance of alarms and warning systems designed to alert personnel to emergency situations, and the potential hazards associated with tampering and misuse of these systems. According to one of the referenced ORPS reports, a Final Safety Analysis Report describes the LS/DW as the most critical alarm system at Rocky Flats. Facility management should ensure that the safety significance of tampering and misuse of these systems is effectively communicated to site personnel. 9. WORKER BURNED FROM ENERGIZED WIRE On September 21, 1993, a worker in Building 710 at the Nevada Test Site received minor burns while she was working in an energized junction box. The employee was adding ground wires to an air conditioning circuit and pulled a wire with a pair of pliers. The pliers cut through the insulation and contacted the side of a junction box. A short circuit resulted and caused minor flash burns on the worker's hands. She was transported to a medical facility, treated, and released. Facility personnel are investigating the event for identification of cause, corrective actions, and lessons learned. (ORPS Report NVOO-- REEC-OMD6-1993-0003) A number of personnel injuries and near misses from electric shock have been reported by other DOE facilities. A recent near miss occurred on August 18, 1993, at the Los Alamos National Laboratory Physics Complex when an electrician came in contact with a live 440-volt ac bus and ground with a wrench causing a substation breaker to trip. This resulted in a loss of power to a portion of the facility. Although no personnel injuries or equipment damage resulted from this event, there was a potential for serious injury or fatality (ORPS Report ALO-LA-LANL-PHYSCOMPLX-1993-0006). On May 22, 1992, a technician at the Lawrence Livermore National Laboratory received an electrical shock while connecting a cable between equipment and a high-voltage power supply that had not been de-energized (ORPS Report SAN--LLNL-LNL-1992-0055). In another event on September 9, 1992, two electricians at Rocky Flats Building 707 received flash burns to their hands when an allen wrench used by one to tighten a ground lead slipped and made contact with an energized 480-volt bus bar. The post incident investigation determined that the electricians were not working in compliance with electrical safety requirements contained in the facility Health and Safety Practice Manual (ORPS Report RFO--EGGR-PUFAB-1992-0248). On November 5, 1990, an electrician at the Pinellas Plant received an electrical shock when he made contact with a 480-volt bus as he tightened a conduit lock nut on a switch. The electrician did not check for energized equipment before putting his hand on the switch (ORPS Report ALO-PI-GEND-PINELLAS-1990-0036). These events emphasize the importance of incorporating industry standard electrical safety practices into work habits and work planning. Failure to do so can result in serious personnel injuries or fatalities. Continuing training on electrical safety methods for all personnel working on electrical equipment should be considered. Information on industry standard practices for electrical safety may be found in American National Standards Institute/Institute of Electrical and Electronic Engineers (ANSI/IEEE) C2, National Electrical Safety Code. ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES 1. IDAHO TEST REACTOR AREA HOT CELL RADIATION STREAMING EVENT CORRECTIVE ACTIONS In OE Weekly Summary 92-11, NS described an event at the Test Reactor Area Hot Cell (TRAHC) facility in Idaho where on March 18, 1992, facility personnel discovered a radiation stream measuring 2 rem/hour from a hot cell wall. The radiation stream was discovered during a routine radiation survey being conducted in conjunction with Cobalt- 60 processing in the hot cell. Radiation protection personnel traced the stream to a small collimator opening (1/2 inch by 3/4 inch) in the four-foot thick shielding wall. The stream was produced when the Cobalt-60 being processed in the cell was positioned directly in line with the collimator. (ORPS Report ID--EGG-TRAHC-1992-0003) An investigation into the event lead to the determination that an Unreviewed Safety Question (USQ) existed based on the lack of a bounding analysis for radiation exposure to a TRAHC worker. The determination of a USQ required that the facility be placed in a shutdown condition pending Type 2 restart approval. In September, 1993, NS received the following information from TRAHC personnel describing activities that have taken place since the facility was shut down. As a result of the event a detailed corrective action plan was developed for facility recovery. The recovery strategy addressed all areas of facility operations including management, technical safety basis, material condition, procedures, conduct of operations, radiological improvements, and detailed operator retraining. The management organization was revised by the contractor to more directly include the TRAHC facility into the Power Reactor Program (RPT) Group and Department level organizations. The facility Safety Analysis Report (SAR) and Technical Safety Requirement (TSR) documents were completely rewritten to conform to DOE Order 5480.23 and 5480.22. The contractor completed an "as built" review of all necessary facility drawings and completed repairs of all electrical and ventilation systems. All cell shielding was inspected and upgraded as required to restore it to original construction design, and detailed radiation surveys were conducted to establish a safety basis for operation. All facility operating procedures were rewritten incorporating appropriate radiological, safety, and conduct of operations requirements, and these procedures were included into the Department's process for configuration control. The facility was extensively cleaned, decontaminated, and repainted. As a result, the incidence of contamination events has decreased by more than 80%. Notable ALARA improvements in operations have reduced personnel exposure for cell entries by a factor of seven. An historical dose evaluation was completed to estimate TRAHC personnel exposure from any historical streaming events. A facility wide automated dosimetry tracking system has been implemented to efficiently monitor and control both personnel and total job exposures. The facility training and qualification programs were revised in accordance with the requirements of DOE Order 5480.20 and all personnel in the facility were re-qualified. The re-qualification process placed considerable emphasis on conduct of operations philosophy, facility safety basis documentation, and procedure changes made to support TRSs. Long range training plans were developed and put in place to conduct ongoing training in conduct of operations and radiological safety. These recovery activities have restored the operational safety and reliability of the facility. A thorough review of the facility status was recently completed during a Operational Readiness Review (ORR). The small number of minor findings made during the ORR indicate that the contractor management has successfully corrected the issues which led to the facility shutdown, and have established a new standard of material and personnel performance readiness. SAFETY NOTICES UNDER DEVELOPMENT Note: The Office of Nuclear Safety encourages input related to the development of Safety Notices. If you have any questions, comments, or information concerning events or issues similar to the following, please contact Mr. Dick Trevillian, Office of Nuclear Safety at (301) 903-3074. 1. NS has identified a number of events related to the loss of annunciators and other safety-related equipment because of problems involving 120-VAC/125-VDC systems at DOE and commercial facilities. NS is reviewing potential generic problems associated with the adequacy of 120-VAC/125-VDC systems at DOE facilities. 2. NS evaluated three events associated with the temporary diesel generator at the Rocky Flats Plant, Building 707. The lessons learned from these events, particularly as they relate to the control of temporary modifications, are being considered for dissemination in an NS Safety Notice. 3. NS is developing a Safety Notice concerning problems with Uninterruptible Power Supplies (UPS). 4. NS is considering development of a Safety Notice related to control of work at electrical substations and switchyards. 5. NS is working with Lawrence Livermore National Laboratory and DOE-SF personnel to develop a Safety Notice on cracking in ventilation ducting. 6. NS is considering developing a Safety Notice related to fuel oil supplies for Emergency Diesel Generators (EDGs). 7. NS is developing a Safety Notice to address uses of independent verification for equipment positioning. 8. NS is developing a Safety Notice related to maintaining important alarm and monitoring systems at facilities undergoing transition and decontamination and decommissioning. SAFETY NOTICES PREVIOUSLY ISSUED Safety Notice No. 91-1, "Criticality Safety Moderator Hazards," September 1991 Safety Notice No. 92-1, "Criticality Safety Hazards Associated With Large Vessels," February 1992 Safety Notice No. 92-2, "Radiation Streaming at Hot Cells," August 1992 Safety Notice No. 92-3, "Explosion Hazards of Uranium-Zirconium Alloys," August 1992 Safety Notice No. 92-4, "Facility Logs and Records," September 1992 Safety Notice No. 92-5, "Discharge of Fire Water Into a Critical Mass Lab," October 1992 Safety Notice No. 92-6, "Estimated Critical Positions (ECPs)," November 1992 Safety Notice No. 93-1, "Fire, Explosion, and High-Pressure Hazards Associated with Drums and Containers," February 1993 Copies of NS Safety Notices may be requested from: Nuclear Safety Information Center, Office of Nuclear Safety, U.S. Department of Energy, Room S161, GTN, Washington, DC 20585