NS OPERATING EXPERIENCE WEEKLY SUMMARY 93-2
                      January 8 - January 14, 1993


     The purpose of the NS Operating Experience (OE) Weekly Summary is to enhance
     safety throughout the DOE complex by promoting the feedback of operating experience
     and by encouraging the exchange of information among DOE nuclear facilities.  The OE
     Weekly Summary is distributed for information only.  No specific actions or responses
     are required solely as a result of this document.

     Readers are cautioned that review of the OE Weekly Summary should not be relied
     upon as a substitute for a thorough review of the interim and final Occurrence Reports.

     The following events were reviewed during the week of January 8 - January 14, 1993.

    ITEM                                               PAGE


    1. ADMINISTRATIVE RADIATION EXPOSURE LIMITS EXCEEDED     1
    2. LOSS OF CRITICALITY CONTROL AT FUEL FABRICATION FACILITY   2
    3. TANK OVERFLOW AT SRS H-CANYON                    3
    4. OVERHEATED PRODUCTION CELL                       3
    5. CONTAMINATED HAND INJURY IN GLOVE BOX            4
    6. DIVERSION VALVE FAILS FUNCTIONAL CHECK           5
    7. CRYSTALLIZATION OF POTASSIUM HYDROXIDE (KOH) 
       IN PIPE CAUSES PUMP FAILURE                      5
    8. CONFINED SPACE ENTRY WITHOUT REQUIRED PERMITS    5
    9. UNAUTHORIZED CRANE MODIFICATION CAUSES NEAR MISS 6
    10.    SEVERE HAND INJURY FROM IMPROPER POWER TOOL MAINTENANCE     7
    11.    FIRES AT CHERNOBYL                           8
    12.    ELECTRICAL FAILURE IN HAWORTH  POWERED PANEL 8



    1. ADMINISTRATIVE RADIATION EXPOSURE LIMITS EXCEEDED

       On January 8, 1993, dosimetry personnel at Hanford determined that five employees
       had exceeded their administrative Lifetime Control Level (LCL) of N rem where N is
       the age of the employee in years.  The dosimetry personnel notified the employees
       and facility managers.  Facility managers placed the employees on radiation work
       restriction pending the establishment of special control levels in accordance with
       Article 216 of the Radiological Control Manual (RCM) (ORPS REPORT RL--WHC-WHC200EM-
       1993-00030).

       The LCL of N rem and the methodology for calculating total dose were recently
       established by the DOE RCM (DOE N 5480.6, effective June 1992).  Prior to this, the
       total dose was calculated by summing an individual's external dose (documented TLD
       readings etc.) and the person's annual effective dose equivalent from internal
       depositions.  However, the revised administrative limit defines total dose as the sum
       of the individual's external dose plus his 50 year committed dose from internal
       depositions.  The 50 year committed dose is defined as the dose rate due to the
       deposition, calculated over the fifty year period following the deposition.  The total
       dose for the fifty years is assigned to the current year (year of the deposition) totals.

       Consider an example:  A radiation worker age 58 (therefore with an LCL of 58 rem)
       has a lifetime accumulated dose of 10 rem, an internal deposition exposure of 1 rem
       and a current year external dose of 3 rem.  His total dose used to be calculated as
       follows:  a previous total of 10 rem, plus 1 rem internal dose from current the
       contribution, plus the current external dose of 3 rem,  for a total of 14 rem or 44 rem
       less than his LCL.
    
       Article 212 of the RCM now requires that his dose be calculated as follows; 10 rem
       previous total, plus 3 rem current external dose plus perhaps 50 rem committed dose
       equivalent.  The actual 50-year committed dose equivalent will depend on the
       biological half-life of the ingested contaminant plus other factors. The total thus
       becomes 63 rem.  The worker exceeds his LCL of 58 rem by 5 rem and must be
       placed on radiation work restriction.

       Article 216 of the RCM allows for establishing special control levels provided certain
       requirements are met.  For example, special controls may be established when the
       worker's remaining natural life span is less than 50 years (as would be the case in the
       example above).

       10#CFR#20 was revised to contain similar changes affecting the commercial nuclear
       industry radiation worker.  These changes incorporate advances in scientific
       knowledge and implement the 1987 presidential guideline on occupational radiation
       exposure.

       Changes brought about by implementation of the DOE RCM need to be reviewed with
       radiation protection personnel in detail, because the description given above is only
       a simplified example of the effects of the changes.  As the nuclear industry strives
       to improve the protection of exposed workers, it is essential to stress and implement
       the ALARA concept to meet these challenges.  ALARA should be a major
       consideration in every work plan. 


    2. LOSS OF CRITICALITY CONTROL AT FUEL FABRICATION FACILITY

       On January 12, 1992, personnel at a General Atomics uranium fuel fabrication facility
       in San Diego, California notified the NRC of a loss of a criticality barrier.  General
       Atomics manufactures fuel for TRIGA research reactors at this facility.  One step in
       the process involves melting a zirconium-uranium metal mixture in an induction heated
       mold inside a casting furnace.  The mold is surrounded by insulation and a water
       cooled jacket.  A mold heated to approximately 1900 degrees centigrade in the
       furnace, developed a pin-hole leak in the water-cooled jacket allowing water to enter
       the insulation.  The water flashed to steam causing the mold to be ejected out of its
       holder and the molten metal mixture to be dispersed inside the furnace.  Because of
       the limited quantity of uranium in the batch, there was no possibility of a criticality
       accident existed.  However, dispersement of the metal mixture constituted a loss of
       geometry and therefore a criticality control violation.  All material was contained
       inside the furnace.  (NRC event number 24865)


       As part of its investigation of this event, the NRC noted that the facility s safety
       analysis report (SAR) did not consider this accident scenario and had therefore not
       analyzed the potential consequences.  This event serves as a reminder for DOE
       nuclear facility personnel to ensure that all credible accident scenarios are identified
       and analyzed in their facility s SAR.  Information on criteria for nuclear SARs can be
       found in DOE Order 5480.24,  Nuclear Safety Analysis Reports. 


    3. TANK OVERFLOW AT SRS H-CANYON

       On January 7, 1993, at the Savannah River Site's (SRS) H-Canyon 211 H facility, an
       operator noticed the E-3-3 holding tank level stabilize, then begin to decrease
       unexpectedly, during a routine transfer of potentially contaminated rainwater from the
       F-1-6 catch basin sump to the tank.  The operator immediately stopped the transfer
       and sent another operator to inspect the tank area.  The second operator reported the
       tank was overflowing.  The overflow drained back to the F-1-6 sump so no cleanup
       was required.

       The operator had verified the tank level on a computer screen before starting the
       transfer to ensure sufficient tank volume was available, as called for by the facility
       procedure.  Preliminary investigation discovered that, while the level detector
       operated correctly, either the level transmitter or the data link to the computer screen
       had failed. The time and reason for either failure is currently under investigation; these
       level instruments are included in the facility's measuring and test equipment program.

       Although the tank overflowed, the operator demonstrated good conduct of operations
       practice regarding equipment monitoring and responding proactively to indicators. 
       The operator was alerted to this event by monitoring the level indication, and if she
       had not noticed it, the cycle might have continued for a much longer time.  Facilities
       need to encourage a similar level of attention to detail and a questioning attitude by
       their operators. 


    4. OVERHEATED PRODUCTION CELL

       On January 7, 1992, operator inattention and failure to completely restore from
       maintenance testing caused a production cell to overheat at the Paducah Gaseous
       Diffusion Plant.  Operations and Instrument Maintenance personnel were conducting
       routine maintenance testing of coolant and seal system alarm setpoints.  As part of
       the testing, operators placed a pneumatic controller in the  seal  mode.  Placing the
       controller in this mode seals the air pressure to the control valve, and the valve will
       either remain in the same position or move if pressure in the air line decreases.  After
       completing the test, operators did not return the controller to its normal position. 
       Because the test was performed routinely by trained personnel, there was no
       procedure or checklist for system restoration following the test.

       Some time later, a local cell monitoring system alarmed in the control room.  The
       alarm was indicated by an alarm printer, an annunciator light, and an audible general
       alarm.  Facility personnel silenced the available alarm, assuming alarm testing was still
       in progress.  The control room operators did not realize an actual alarm condition
       existed until about 50 minutes later.  Other alarm testing activities being conducted
       at the same time may have contributed to the unrecognized alarm condition.  Control
       room operators then dispatched an operator to the local cell panel.  The operator 


       arrived at the local panel and noticed that the cell temperatures were above the
       operating limit.  Operators then shut down the cell in accordance with facility
       procedures.  (ORPS Report ORO--MMES-PGDPCASOPS-1993-0001)

       No damage to the cell resulted from the overheated condition.  Had the operators not
       identified the alarm condition and shut down the cell, the cell monitoring system was
       designed to automatically shut down the cell when a high coolant pressure setpoint
       was reached.  

       This event emphasizes the need for operators to be especially alert to the possibility
       that alarm testing could mask actual alarm conditions.  Every alarm should be verified
       prior to acknowledging and silencing.  The event also illustrates the benefits of using
       procedures or checklists when conducting testing activities, even routinely performed
       tests.


    5. CONTAMINATED HAND INJURY IN GLOVE BOX 

       On January 6, 1993, at Argonne National Laboratory-West (ANL-W), a laboratory
       worker, preparing a glovebox for decontamination, cut his hand and contaminated the
       wound (ORPS Report CH-AA-ANLW-1993-0001).  The worker was preparing pieces of a
       broken glass beaker and other miscellaneous items for removal from the glovebox. 
       He was attempting to wrap duct tape around a plastic bag containing the broken
       glass to prevent sharp edges from damaging the outer bag-out sleeve and to maintain
       a 9-inch dimensional limit to permit passage through the access door.  Wrapping
       contaminated sharp objects with tape to prevent damage to vinyl bag-out sleeves is
       a standard practice at ANL-W. 

       While wrapping the bag, the worker's hand slipped and the resultant impact caused
       a piece of glass to penetrate the bag and the worker's glove in the glove port.  The
       worker sustained a puncture wound on his right palm.  An ANL-W Radiation Safety
       technician found contamination in the wound.  After the contamination was reduced
       to about 100 counts alpha, the worker went to a central dispensary for continued
       decontamination and treatment.  Additional gamma monitoring of the injured hand
       was negative and a whole body count was normal.  Bio-assay samples were also
       collected to determine whether any measurable uptake occurred.

       In the future, ANL-W personnel plan to use metal containers to collect contaminated
       broken glass, and their lids will be taped down prior to placement in the vinyl bag-out
       sleeve.  The facility is phasing in the use of metal beakers.

       OE Weekly Summary 92-36 reported a similar event at the Savannah River Tritium
       Facility.  On December 20, 1992, an operator removing a small O-ring from a
       contaminated component with a dental-pick probe, slipped and punctured the anti-
       contamination glove on his left hand, breaking the skin on his palm (ORPS Report SR--
       WSRC-TRIT-1992-0069).

       These events point out the importance of using extreme care when working with
       sharp objects in a radiation contaminated environment.  A wound sustained under
       such circumstances can be difficult to decontaminate.  Facilities should consider
       alternate methods of handling contaminated sharp objects and substitute, where
       possible, unbreakable laboratory equipment for glovebox use.



       6.  DIVERSION VALVE FAILS FUNCTIONAL CHECK

       On January 10, 1993, an electrically powered diversion valve at the Savannah River
       F-Canyon failed to operate during a weekly functional check.  Facility personnel were
       also unable to manually operate the valve (ORPS Report SR--WSRC-FCAN-1993-0002). This
       failure is significant because the diversion valve redirects canyon cooling water to a
       retention basin if high activity is detected in the cooling water. During normal
       operation, the cooling water is either recirculated through a cooling tower or
       discharged into a creek feeding into the Savannah River. Until the valve is repaired,
       operators can manually divert the cooling water by using several system drain valves. 

       Facility personnel have categorized this valve as a Critical Protection component and
       operators functionally test it on a weekly basis. During troubleshooting efforts,
       maintenance personnel identified a failed shear pin on the Limitorque valve actuator
       which prevented valve operation. Facility personnel are investigating the cause of the
       pin failure. NS will follow this item and report as necessary on the cause of the shear
       pin failure.


    7. CRYSTALLIZATION OF POTASSIUM HYDROXIDE (KOH) IN PIPE CAUSES PUMP
       FAILURE

       On December 30, 1993, at the Hanford Uranium Oxide (UO3) Facility, a Condensate
       Neutralization system pump failed because KOH solidified in a pipe line.  In addition,
       a manual valve downstream of the pump could not be operated because of the
       solidified KOH (ORPS Report RL--WHC-UO3-1993-0002).

       Facility personnel replaced the affected pump and valve and restarted the system on
       January 7, 1993.  Investigation determined that changing from 45 WT% KOH to 50
       WT% KOH had caused the solidification.  Facility personnel had recently begun using
       50 WT% KOH because a surplus of this concentration was available from an adjacent
       facility.

       Recent abnormally cold weather at the Hanford Site contributed to the occurrence. 
       Because of UO3 facility plans to continue using 50 WT% KOH, facility personnel
       covered the KOH tank and relevant piping with steam jacketing.

       This event involves fundamental chemical and process engineering problems.  Before
       a solution concentration or a weight percentage is changed, the modification must be
       evaluated, taking into consideration such things as system pressures, ambient
       temperatures, pumping requirements, etc. to ensure that the process will not be
       degraded by the proposed modification.  When facilities, for economic reasons, take
       advantage of excess supplies with different characteristics than had been used
       before, a thorough engineering review of potential deleterious effects is required to
       help prevent unnecessary downtime and equipment replacement.  


    8. CONFINED SPACE ENTRY WITHOUT REQUIRED PERMITS

       On January 6, 1993, Health Physics (HP) technicians at the Idaho Chemical
       Processing Plant (ICPP) entered the CPP-604 WL-101/102 vault and performed a
       comprehensive radiation and contamination survey.  The technicians did not have a
       completed Hazardous Work Permit (HWP) for the vault entry.  An Operations Shift 


       Manager (SM) and an HP Supervisor approved the vault entry.  The HP technicians
       wore supplied-air respirators and personnel extraction gear.  A back-up extraction
       team stood by the access hatch during the entry.

       The survey was a part of the pre-job activity called for in a Special Procedure (SP)
       (CPP-604 WL-101/102 "Vault Decontamination") to decontaminate the vault to allow
       a construction contractor to line the vault floors and wall to comply with the
       Resource Conservation and Recovery Act.  The SP directed all activities necessary to
       complete the job.  It included a pre-job survey and required that HP technicians obtain
       an HWP.  The SM who approved the entry for the survey had himself initiated a
       request for an HWP for the work.  The HP technicians submitted the HWP request to
       the Industrial Safety supervisor for review and approval.  He told them that more
       steps needed to be completed before he could approve the HWP.  The HP technicians
       reportedly thought the pre-job survey was one of the steps to be completed before
       the HWP could be approved.  Before the SM approved the entry, he asked the
       technicians whether they had everything they needed (including the HWP). They
       responded that they did, thinking that the survey needed to be done to get the HWP
       approval.

       The requirements for issuing an HWP include an atmosphere survey for oxygen
       concentration, a pre-job briefing, extraction gear, and the staging of a back-up
       extraction team at the access point.  All the elements required for the HWP were in
       place, with the exception of the atmosphere sampling and the pre-job briefing. 
       Because the technicians wore supplied-air respirators, the lack of an atmosphere
       sample was considered insignificant.  No injuries resulted from the event.

       The WL-101/102 vault, a concrete shell, contains two waste holding tanks.  One of
       the tanks holds intermediate waste water for processing through process equipment
       waste (PEW) evaporators.  The other tank receives the concentrated waste after
       processing.  Potential hazards associated with entry into this vault include nitrous
       oxide gas, radioactive gases, airborne radioactive contamination and an oxygen
       deficient atmosphere.

       The cause of this event was a breakdown in communications between the SM, the
       Industrial Safety supervisor and the HP Technicians.  The involved personnel assumed
       important information rather than communicating and verifying it.  This event
       illustrates the importance of complete communications, including repeating back
       essential items.  In this case no one was injured because the technicians used the
       appropriate equipment and back-up personnel were on hand, and no hazard was
       present at the time.  Facilities should use procedures to avoid reliance on memory and
       assumption, but without adequate communications even the procedures will not
       always be sufficient to ensure a safe approach to the job.


    9. UNAUTHORIZED CRANE MODIFICATION CAUSES NEAR MISS

       On December 11, 1992, at the Argonne National Laboratory-East Plant Facilities
       Services (PFS) area, an assembly consisting of a piece of Unistrut  and an iron casting
       weighing approximately seven pounds fell about 15 feet from an overhead 4-ton
       bridge crane trolley.  The assembly missed hitting a plant employee by less than two
       feet.  The assembly had been attached to the overhead crane as a trolley travel stop. 
       It was not part of the original trolley design nor was it an authorized modification of
       it.


       Facility personnel stopped the crane and locked it out of service.  PFS crane
       maintenance and safety personnel reconstructed the incident and found that two
       modifications had been made to the crane.  The first modified the power connector
       follower attached to the bridge.  The hoist is the only electrically operated component
       of this crane.  It requires a power cable and connector that must track with the bridge
       and trolley to provide power to the hoist motor.  A chain attaches the connector to
       the bridge.  For unknown reasons the chain had been shortened, thus bringing the
       connector within the trolley's range of travel.

       The second modification added the Unistrut  and casting assembly that fell from the
       trolley.  This "home made" trolley stop apparently had been installed because the
       trolley had been contacting the hoist power connector before reaching the
       manufacturer installed trolley stop, apparently due to the first modification.

       The crane maintenance group re-located the power connector out of the trolley travel
       path.  The manufacturer installed trolley stop functioned properly with the hoist cable
       power connector in its correct location.  Facility personnel could not determine when
       the modifications had been made.

       This event illustrates that unauthorized modifications to facility equipment may cause
       equipment failures.  Facility modification procedures provide a formal method for
       review, approval and documentation of changes to facility components, systems or
       structures.  Bypassing any of these steps can create hazardous conditions.  Review
       and approval of facility modifications, whether permanent or temporary, should
       include consideration of potential impacts on facility procedures, training,
       procurement, maintenance, operations and safety.


    10.    SEVERE HAND INJURY FROM IMPROPER POWER TOOL MAINTENANCE

       On January 6, 1993, at Lawrence Livermore National Laboratory, an employee was
       cleaning and inspecting a rotating grinding wheel and cutting blade when the small
       and ring fingers of his left hand were severed (ORPS Report SAN--LLNL-LLNL-1993-0001). 
       The employee inadvertently placed his hand in a position where the rotating wheel
       pulled his fingers into a point where they were pinched with the knife edge.  Normal
       operating practice requires the blade to be backed away from the grinder prior to
       inspection.  There was no written procedure for this task.  Also, machine guards did
       not fully cover the blade/grinding wheel area.  The injured employee was transported
       to a local hospital where both fingers were reattached.  Facility personnel locked and
       tagged the machine out of service, and began a lab wide survey of machine tool
       guarding.

       All machine tool equipment should be inspected and evaluated for compliance with
       OSHA safety standards.  Facilities should provide employees engaged in operation
       and maintenance of machine tools with necessary training and up to date procedures
       or instructions that address safety hazards.  The risk of severe injury may be reduced
       by establishing various barriers to prevent rotating machine hazardous parts from
       contacting worker's hands, etc.  These barriers usually inspection to ensure
       compliance with applicable standards, training of operators and maintenance
       personnel, and written precautions.





    11.    FIRES AT CHERNOBYL

       On January 13, 1993, a small fire broke out at the Chernobyl nuclear power station
       located 80 miles north of Kiev, Ukraine.  Ukrainian nuclear officials stated that the fire
       occurred in a room between the station's first and second reactors and was quickly
       brought under control. There was no change in radiation levels at the facility. 
       Although the cause of the fire is under investigation, officials speculate that the blaze
       could have been started after melted snow dripping from the roof caused a short
       circuit in an auxiliary electrical unit that supplied power to welding equipment.  The
       fire did not affect the two operating reactors at the site.  On January 14, 1993,
       another fire occurred in the ventilation corridor above the cement sarcophagus that
       covers the Unit No. 4 reactor core.  Site personnel quickly extinguished the blaze and
       no radiation was released.  This is the fourth blaze reported at the Chernobyl complex
       since the April 1986 explosion and fire spread radiation over a wide section of
       Ukraine and Belarus.  Another fire in November 1991 damaged the generator room
       of reactor No. 1 (Newswire Service).


    12.    ELECTRICAL FAILURE IN HAWORTH  POWERED PANEL

       On January 4, 1992, in the Drafting Office area at Sandia National Laboratory's
       Livermore Site, employees heard a breaker trip and simultaneously witnessed a spark,
       then a flash, from a power connector at the bottom of a Haworth  Powered Panel
       System panel.  This system is a room divider with electrical power outlets in the
       raceway at the base of each panel.  The employees found a small scorched area on
       each side of the panel, and the plastic connector was partially melted (ORPS Report ALO-KO-
       SNL-LVMRSITE-1993-0001).  A similar occurrence was reported in UOR-90-17, dated 5/14/90.

       These panels have been in service at this site for about ten years.  They are designed
       for a 20-amp load.  However, the manufacturer recommends a 16 amp load for
       extended use.  On the morning of January 4, 1993, employees had just returned from
       holiday.  Six employees powered up their work stations, i.e. computers, desk lights,
       etc.  One employee plugged in a 13-amp heater because it was cold in the area.  This
       additional electrical load apparently caused the failure of the panel.

       One of the most common hazards in the home or the work place is overloading of
       electrical outlets.  (Electrical load in amps can be determined by dividing the device
       nameplate wattage by the circuit voltage.)  In this case, a 1500-watt heater drew
       about 13 amps (1500 watts divided by 115 volts).  In the last decade, increased use
       of electrical equipment in the work place has challenged the capacity of many
       electrical circuits.  Facility personnel should ensure adequate margins of safety are
       maintained for partitions containing circuits and electrical outlets, especially if they
       service work station locations.



    ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES

    1. ADDITIONAL LOCK-OUT/TAG-OUT NONCOMPLIANCES

       Lock out/Tag out (LO/TO) problems were the subject of recent items in the NS
       Operating Experience Weekly Summary (Inadequate Interface Between Construction
       and Operations Tag-outs, NS 92-33; Improper Lock-out/Tag-out Incidents, NS 92-35). 
       Two recent events at Hanford merit this follow-up report.

          On January 8, 1993, in the Hanford tank farms, a work package was released
           to perform work related to the installation of an emergency diesel generator at
           Building 701-A. A LO/TO was approved and installed on day shift except for
           final verification which was to consist of an independent check of the LO/TO
           by an operator and a supervisor.  Due to a shift change and the fact that the
           actual work was performed by contractor personnel, the work commenced
           without the required final verification being done.

          On December 28, 1992, at the Plutonium Finishing Plant, a LO/TO was installed
           to assure the de-energizing of a breaker on an electrical panel.  Later, the LO/TO
           Custodian allowed the LO/TO tags to be removed for switch testing by
           electricians.  After testing, the LO/TO tags were re-hung without the required
           independent verification of the LO/TO.  Over the next ten days the LO/TO tags
           were removed and replaced two more times.  

       In both of these cases managers recognized after the fact that a procedural violation
       had occurred.  In dealing with LO/TO situations, compliance with procedures is
       MANDATORY to assure personnel safety.  Where work extends over several shift
       crews, and contractor personnel are involved in performing maintenance tasks,
       communication is vital to ensure that procedural requirements are completed before
       the work is initiated.


    2. FOLLOW-UP ON LITHIUM FIRE IN WASTE HANDLING FACILITY

       OE Weekly Summary 92-36 reported a lithium fire on December 14, 1992, at the
       Lawrence Berkeley Laboratory (LBL), as contractor personnel were preparing lithium
       ribbon for packing.  The lithium was being prepared by immersion in methanol inside
       a fume hood designed for handling hazardous materials.  The lithium ignited as it was
       being immersed in the methanol (ORPS Report SAN--LBL-EHS-1992-0012).

       Additional information indicates that mineral oil should have been used for immersing
       the lithium, since methanol is readily miscible with water.  The site disposal guide
       used by contractor employees performing the work merely called for "a solvent"
       rather than specifying mineral oil.

       Two additional lessons were learned by the LBL staff from their review of this
       incident.  First, the generator of the waste lacked the training and knowledge to
       package the lithium correctly, as evidenced by the fact that he had left it in a bag
       under the fume hood.  Had he placed the lithium properly in mineral oil, the contractor
       personnel responsible for waste disposal would not have had to attempt to immerse
       it themselves.

       Second, the contractor personnel should not have attempted to prepare it for disposal
       without notifying the responsible individual that it had not been packaged correctly. 
       The contractor was a certified waste handler, but his procedure was in error. 
       Vendors have been required to change procedures and retrain their personnel.  In
       addition, LBL staff will now provide strict oversight of vendor staff during the
       collection, transfer, and packaging of waste.

       Facilities that routinely handle combustible metals should ensure that employees are
       trained in extinguishing metal fires.  A good reference would be the National Fire
       Protection Association Standard (NFPA FPH SEC 5-21), "Combustible Metal
       Extinguishing Agents and Application Techniques."

    3. FOLLOW-UP ON DIESEL GENERATOR CYLINDER HEAD PROBLEMS

       OE Weekly Summary 92-32 discussed problems reported by Gulf States Utilities
       (GSU) regarding potential problems in Type R-4 diesel generators (DGs) under the
       manufacturer name Enterprise Engine Company or IMO-DeLaval.  Cooper-Bessemer
       has since acquired IMO-DeLaval and now has the responsibility of notifying owners
       of the suspect cylinder heads. (NRC EN 24655).  Cylinder heads in these DGs cast
       before August 1, 1984 may have inadequately thick walls.  The problem was
       discovered during an investigation at the River Bend nuclear power plant on October
       15, 1992.  On that date a diesel generator was taken out of service to investigate
       traces of engine coolant found in lubricating oil samples.  The source of the coolant
       was identified to be a minute leak from the number four cylinder head into the valve
       train area, where it drained to the engine base.  This event is documented in a 10
       CFR Part 21 report (#92-248) to the NRC dated November 16, 1992.

       On December 17,
       1993, Cooper-
       Bessemer provided
       further identification
       of the affected heads
       to the NRC and
       owners of their
       diesel engines.  The
       final report identifies
       affected heads by
       serial number and
       contains recom-
       mended corrective
       action.

       The root cause for
       the failure at GSU
       was inadequately
       thick cast walls at
       the 3/4"-10 bolt hole
       indicated on a sketch
       supplied for the 10
       CFR Part 21
       notification (Figure
       1).  Cooper-Besse-
       mer Design
       Engineering has
       reviewed the design 
       drawings to determine whether any other sub-cover bolt holes do not have adequately
       thick walls between the bolt hole and the adjacent water passage.  Their review
       revealed no other bolt holes with inadequate wall thickness.

       The affected cylinder heads are identified by one of the following part numbers: 03-
       360-03-0F, 1A-6446, 1A-6447, 1A-6879, 1A-6240, 1A-6239, 1A-7062, 1A-5559,
       1A-5558, 1A-6266, or 1A-6265, all of which were  cast prior to August 1, 1984.





       Identification of individual heads may be accomplished by referring to Figure 1 and
       from the following information:

           All heads have the cast serial number, heat number, cast date,
           manufacturing date, water test, air test, gas test, and possibly
           reconditioning information stamped on the head.  At Area 1 on Figure 1,
           which is inside the sub-cover, the serial number, heat number and cast date
           should be stamped with minimum of ¨" size letters.  Area 2 on Figure 1,
           which is outside the sub-cover on the head, includes serial number, heat
           number, manufacturing date, water test, air test, gas test information and
           possibly reconditioning data.

       Area 1 should be examined for the cast date as stamped by the Enterprise foundry
       with steel stamps.  This may be difficult to see as this area has been painted.  Other
       clues to the age of the cylinder head are at Area 2. If the serial number is L99 or less,
       and the manufacturing date is before 1986, it is most likely a cylinder head cast prior
       to August 1, 1984.  Any questions concerning cast dates and serial numbers should
       be directed to John R. Schneider, Manager, Quality Assurance at 412-458-3434.

       Corrective action includes removing the stud at the location shown in Figure 1 and
       applying Loctite  Hydraulic Sealant (Item No. 56931) or equivalent, per Loctite  instru-
       ctions, to the threaded hole and stud.  Tests at Cooper-Bessemer conducted on
       December 7, 1992, proved this repair sufficient to withstand 100 psi of water
       pressure (hot or cold) without leakage.  Cooper-Bessemer Service Information Memo
       #384 is being issued which explains this procedure in more detail.  This corrective
       action should be performed at the next scheduled diesel engine outage.

       Corrective action at Cooper-Bessemer will be to repair this head section on all
       affected cylinder heads returned to them for rebuilding or repair, using their standard
       repair EAR-11-001. This involves drilling the hole 1/8" oversize and 1/8" deeper,
       filling the hole completely with weld metal, redrilling and re-tapping to blueprint size
       and depth, and re-hydrotesting.

       Managers of DOE facilities with Type R-4 DGs manufactured by Enterprise Engine
       Company or their successor, IMO-DeLaval, should determine whether the cylinder
       heads on their units have this problem, and take appropriate remedial actions.




       SAFETY NOTICES UNDER DEVELOPMENT:

        Note:    The Office of Nuclear Safety encourages input related to the development of Safety
                 Notices.  If you have any questions, comments, or information concerning events or
                 issues similar to those described below, please contact Mr. Ivon Fergus, Office of
                 Nuclear Safety (301) 903-6364.

        1. NS has identified a number of events related to the loss of annunciators and
           other safety-related equipment caused by problems involving 120-VAC/125-VDC
           systems at DOE and commercial facilities.  NS is reviewing potential generic
           problems associated with the adequacy of 120-VAC/125-VDC systems at DOE
           facilities.

        2. NS evaluated three events associated with the temporary diesel generator at
           Rocky Flats Plant, Building 707.  The lessons learned from these events,
           particularly as they relate to the control of temporary modifications, are being
           considered for dissemination in an NS Safety Notice.

        3. NS is developing a Safety Notice concerning problems with Uninterruptible
           Power Supplies (UPS).

        4. NS is considering developing a Safety Notice related to control of work at
           electrical substations and switchyards.

        5. NS is developing a Safety Notice related to the handling, storage, venting, and
           opening of containers and drums that may be pressurized or may contain
           flammable vapors.  This notice will contain generic information about proper
           storage conditions and the material conditions of containers.

        6. NS is working with Lawrence Livermore National Laboratory and DOE-SF
           personnel to develop a Safety Notice on cracking in ventilation ducting.

        7. NS is considering developing a Safety Notice related to Emergency Diesel
           Generator (EDG) fuel oil supplies.

        8. NS is developing a Safety Notice addressing uses of independent verification for
           equipment positioning.



        SAFETY NOTICES PREVIOUSLY ISSUED:

        Safety Notice No. 91-1, "Criticality Safety Moderator Hazards," September 1991

        Safety Notice No. 92-1, "Criticality Safety Hazards Associated With Large Vessels,"
        February 1992

        Safety Notice No. 92-2, "Radiation Streaming at Hot Cells," August 1992

        Safety Notice No. 92-3, "Explosion Hazards of Uranium-Zirconium Alloys," August
        1992

        Safety Notice No. 92-4, "Facility Logs and Records," September 1992

        Safety Notice No. 92-5, "Discharge of Fire Water Into a Critical Mass Lab," October
        1992

        Safety Notice No. 92-6, "Estimated Critical Positions (ECPs)," November
        1992


    Copies of NS Safety Notices may be requested from:  Nuclear Safety Information Center,
    Office of Nuclear Safety, U.S. Department of Energy, Room S161, GTN, Washington, DC 
    20585