NS OPERATING EXPERIENCE WEEKLY SUMMARY 93-2 January 8 - January 14, 1993 The purpose of the NS Operating Experience (OE) Weekly Summary is to enhance safety throughout the DOE complex by promoting the feedback of operating experience and by encouraging the exchange of information among DOE nuclear facilities. The OE Weekly Summary is distributed for information only. No specific actions or responses are required solely as a result of this document. Readers are cautioned that review of the OE Weekly Summary should not be relied upon as a substitute for a thorough review of the interim and final Occurrence Reports. The following events were reviewed during the week of January 8 - January 14, 1993. ITEM PAGE 1. ADMINISTRATIVE RADIATION EXPOSURE LIMITS EXCEEDED 1 2. LOSS OF CRITICALITY CONTROL AT FUEL FABRICATION FACILITY 2 3. TANK OVERFLOW AT SRS H-CANYON 3 4. OVERHEATED PRODUCTION CELL 3 5. CONTAMINATED HAND INJURY IN GLOVE BOX 4 6. DIVERSION VALVE FAILS FUNCTIONAL CHECK 5 7. CRYSTALLIZATION OF POTASSIUM HYDROXIDE (KOH) IN PIPE CAUSES PUMP FAILURE 5 8. CONFINED SPACE ENTRY WITHOUT REQUIRED PERMITS 5 9. UNAUTHORIZED CRANE MODIFICATION CAUSES NEAR MISS 6 10. SEVERE HAND INJURY FROM IMPROPER POWER TOOL MAINTENANCE 7 11. FIRES AT CHERNOBYL 8 12. ELECTRICAL FAILURE IN HAWORTH POWERED PANEL 8 1. ADMINISTRATIVE RADIATION EXPOSURE LIMITS EXCEEDED On January 8, 1993, dosimetry personnel at Hanford determined that five employees had exceeded their administrative Lifetime Control Level (LCL) of N rem where N is the age of the employee in years. The dosimetry personnel notified the employees and facility managers. Facility managers placed the employees on radiation work restriction pending the establishment of special control levels in accordance with Article 216 of the Radiological Control Manual (RCM) (ORPS REPORT RL--WHC-WHC200EM- 1993-00030). The LCL of N rem and the methodology for calculating total dose were recently established by the DOE RCM (DOE N 5480.6, effective June 1992). Prior to this, the total dose was calculated by summing an individual's external dose (documented TLD readings etc.) and the person's annual effective dose equivalent from internal depositions. However, the revised administrative limit defines total dose as the sum of the individual's external dose plus his 50 year committed dose from internal depositions. The 50 year committed dose is defined as the dose rate due to the deposition, calculated over the fifty year period following the deposition. The total dose for the fifty years is assigned to the current year (year of the deposition) totals. Consider an example: A radiation worker age 58 (therefore with an LCL of 58 rem) has a lifetime accumulated dose of 10 rem, an internal deposition exposure of 1 rem and a current year external dose of 3 rem. His total dose used to be calculated as follows: a previous total of 10 rem, plus 1 rem internal dose from current the contribution, plus the current external dose of 3 rem, for a total of 14 rem or 44 rem less than his LCL. Article 212 of the RCM now requires that his dose be calculated as follows; 10 rem previous total, plus 3 rem current external dose plus perhaps 50 rem committed dose equivalent. The actual 50-year committed dose equivalent will depend on the biological half-life of the ingested contaminant plus other factors. The total thus becomes 63 rem. The worker exceeds his LCL of 58 rem by 5 rem and must be placed on radiation work restriction. Article 216 of the RCM allows for establishing special control levels provided certain requirements are met. For example, special controls may be established when the worker's remaining natural life span is less than 50 years (as would be the case in the example above). 10#CFR#20 was revised to contain similar changes affecting the commercial nuclear industry radiation worker. These changes incorporate advances in scientific knowledge and implement the 1987 presidential guideline on occupational radiation exposure. Changes brought about by implementation of the DOE RCM need to be reviewed with radiation protection personnel in detail, because the description given above is only a simplified example of the effects of the changes. As the nuclear industry strives to improve the protection of exposed workers, it is essential to stress and implement the ALARA concept to meet these challenges. ALARA should be a major consideration in every work plan. 2. LOSS OF CRITICALITY CONTROL AT FUEL FABRICATION FACILITY On January 12, 1992, personnel at a General Atomics uranium fuel fabrication facility in San Diego, California notified the NRC of a loss of a criticality barrier. General Atomics manufactures fuel for TRIGA research reactors at this facility. One step in the process involves melting a zirconium-uranium metal mixture in an induction heated mold inside a casting furnace. The mold is surrounded by insulation and a water cooled jacket. A mold heated to approximately 1900 degrees centigrade in the furnace, developed a pin-hole leak in the water-cooled jacket allowing water to enter the insulation. The water flashed to steam causing the mold to be ejected out of its holder and the molten metal mixture to be dispersed inside the furnace. Because of the limited quantity of uranium in the batch, there was no possibility of a criticality accident existed. However, dispersement of the metal mixture constituted a loss of geometry and therefore a criticality control violation. All material was contained inside the furnace. (NRC event number 24865) As part of its investigation of this event, the NRC noted that the facility s safety analysis report (SAR) did not consider this accident scenario and had therefore not analyzed the potential consequences. This event serves as a reminder for DOE nuclear facility personnel to ensure that all credible accident scenarios are identified and analyzed in their facility s SAR. Information on criteria for nuclear SARs can be found in DOE Order 5480.24, Nuclear Safety Analysis Reports. 3. TANK OVERFLOW AT SRS H-CANYON On January 7, 1993, at the Savannah River Site's (SRS) H-Canyon 211 H facility, an operator noticed the E-3-3 holding tank level stabilize, then begin to decrease unexpectedly, during a routine transfer of potentially contaminated rainwater from the F-1-6 catch basin sump to the tank. The operator immediately stopped the transfer and sent another operator to inspect the tank area. The second operator reported the tank was overflowing. The overflow drained back to the F-1-6 sump so no cleanup was required. The operator had verified the tank level on a computer screen before starting the transfer to ensure sufficient tank volume was available, as called for by the facility procedure. Preliminary investigation discovered that, while the level detector operated correctly, either the level transmitter or the data link to the computer screen had failed. The time and reason for either failure is currently under investigation; these level instruments are included in the facility's measuring and test equipment program. Although the tank overflowed, the operator demonstrated good conduct of operations practice regarding equipment monitoring and responding proactively to indicators. The operator was alerted to this event by monitoring the level indication, and if she had not noticed it, the cycle might have continued for a much longer time. Facilities need to encourage a similar level of attention to detail and a questioning attitude by their operators. 4. OVERHEATED PRODUCTION CELL On January 7, 1992, operator inattention and failure to completely restore from maintenance testing caused a production cell to overheat at the Paducah Gaseous Diffusion Plant. Operations and Instrument Maintenance personnel were conducting routine maintenance testing of coolant and seal system alarm setpoints. As part of the testing, operators placed a pneumatic controller in the seal mode. Placing the controller in this mode seals the air pressure to the control valve, and the valve will either remain in the same position or move if pressure in the air line decreases. After completing the test, operators did not return the controller to its normal position. Because the test was performed routinely by trained personnel, there was no procedure or checklist for system restoration following the test. Some time later, a local cell monitoring system alarmed in the control room. The alarm was indicated by an alarm printer, an annunciator light, and an audible general alarm. Facility personnel silenced the available alarm, assuming alarm testing was still in progress. The control room operators did not realize an actual alarm condition existed until about 50 minutes later. Other alarm testing activities being conducted at the same time may have contributed to the unrecognized alarm condition. Control room operators then dispatched an operator to the local cell panel. The operator arrived at the local panel and noticed that the cell temperatures were above the operating limit. Operators then shut down the cell in accordance with facility procedures. (ORPS Report ORO--MMES-PGDPCASOPS-1993-0001) No damage to the cell resulted from the overheated condition. Had the operators not identified the alarm condition and shut down the cell, the cell monitoring system was designed to automatically shut down the cell when a high coolant pressure setpoint was reached. This event emphasizes the need for operators to be especially alert to the possibility that alarm testing could mask actual alarm conditions. Every alarm should be verified prior to acknowledging and silencing. The event also illustrates the benefits of using procedures or checklists when conducting testing activities, even routinely performed tests. 5. CONTAMINATED HAND INJURY IN GLOVE BOX On January 6, 1993, at Argonne National Laboratory-West (ANL-W), a laboratory worker, preparing a glovebox for decontamination, cut his hand and contaminated the wound (ORPS Report CH-AA-ANLW-1993-0001). The worker was preparing pieces of a broken glass beaker and other miscellaneous items for removal from the glovebox. He was attempting to wrap duct tape around a plastic bag containing the broken glass to prevent sharp edges from damaging the outer bag-out sleeve and to maintain a 9-inch dimensional limit to permit passage through the access door. Wrapping contaminated sharp objects with tape to prevent damage to vinyl bag-out sleeves is a standard practice at ANL-W. While wrapping the bag, the worker's hand slipped and the resultant impact caused a piece of glass to penetrate the bag and the worker's glove in the glove port. The worker sustained a puncture wound on his right palm. An ANL-W Radiation Safety technician found contamination in the wound. After the contamination was reduced to about 100 counts alpha, the worker went to a central dispensary for continued decontamination and treatment. Additional gamma monitoring of the injured hand was negative and a whole body count was normal. Bio-assay samples were also collected to determine whether any measurable uptake occurred. In the future, ANL-W personnel plan to use metal containers to collect contaminated broken glass, and their lids will be taped down prior to placement in the vinyl bag-out sleeve. The facility is phasing in the use of metal beakers. OE Weekly Summary 92-36 reported a similar event at the Savannah River Tritium Facility. On December 20, 1992, an operator removing a small O-ring from a contaminated component with a dental-pick probe, slipped and punctured the anti- contamination glove on his left hand, breaking the skin on his palm (ORPS Report SR-- WSRC-TRIT-1992-0069). These events point out the importance of using extreme care when working with sharp objects in a radiation contaminated environment. A wound sustained under such circumstances can be difficult to decontaminate. Facilities should consider alternate methods of handling contaminated sharp objects and substitute, where possible, unbreakable laboratory equipment for glovebox use. 6. DIVERSION VALVE FAILS FUNCTIONAL CHECK On January 10, 1993, an electrically powered diversion valve at the Savannah River F-Canyon failed to operate during a weekly functional check. Facility personnel were also unable to manually operate the valve (ORPS Report SR--WSRC-FCAN-1993-0002). This failure is significant because the diversion valve redirects canyon cooling water to a retention basin if high activity is detected in the cooling water. During normal operation, the cooling water is either recirculated through a cooling tower or discharged into a creek feeding into the Savannah River. Until the valve is repaired, operators can manually divert the cooling water by using several system drain valves. Facility personnel have categorized this valve as a Critical Protection component and operators functionally test it on a weekly basis. During troubleshooting efforts, maintenance personnel identified a failed shear pin on the Limitorque valve actuator which prevented valve operation. Facility personnel are investigating the cause of the pin failure. NS will follow this item and report as necessary on the cause of the shear pin failure. 7. CRYSTALLIZATION OF POTASSIUM HYDROXIDE (KOH) IN PIPE CAUSES PUMP FAILURE On December 30, 1993, at the Hanford Uranium Oxide (UO3) Facility, a Condensate Neutralization system pump failed because KOH solidified in a pipe line. In addition, a manual valve downstream of the pump could not be operated because of the solidified KOH (ORPS Report RL--WHC-UO3-1993-0002). Facility personnel replaced the affected pump and valve and restarted the system on January 7, 1993. Investigation determined that changing from 45 WT% KOH to 50 WT% KOH had caused the solidification. Facility personnel had recently begun using 50 WT% KOH because a surplus of this concentration was available from an adjacent facility. Recent abnormally cold weather at the Hanford Site contributed to the occurrence. Because of UO3 facility plans to continue using 50 WT% KOH, facility personnel covered the KOH tank and relevant piping with steam jacketing. This event involves fundamental chemical and process engineering problems. Before a solution concentration or a weight percentage is changed, the modification must be evaluated, taking into consideration such things as system pressures, ambient temperatures, pumping requirements, etc. to ensure that the process will not be degraded by the proposed modification. When facilities, for economic reasons, take advantage of excess supplies with different characteristics than had been used before, a thorough engineering review of potential deleterious effects is required to help prevent unnecessary downtime and equipment replacement. 8. CONFINED SPACE ENTRY WITHOUT REQUIRED PERMITS On January 6, 1993, Health Physics (HP) technicians at the Idaho Chemical Processing Plant (ICPP) entered the CPP-604 WL-101/102 vault and performed a comprehensive radiation and contamination survey. The technicians did not have a completed Hazardous Work Permit (HWP) for the vault entry. An Operations Shift Manager (SM) and an HP Supervisor approved the vault entry. The HP technicians wore supplied-air respirators and personnel extraction gear. A back-up extraction team stood by the access hatch during the entry. The survey was a part of the pre-job activity called for in a Special Procedure (SP) (CPP-604 WL-101/102 "Vault Decontamination") to decontaminate the vault to allow a construction contractor to line the vault floors and wall to comply with the Resource Conservation and Recovery Act. The SP directed all activities necessary to complete the job. It included a pre-job survey and required that HP technicians obtain an HWP. The SM who approved the entry for the survey had himself initiated a request for an HWP for the work. The HP technicians submitted the HWP request to the Industrial Safety supervisor for review and approval. He told them that more steps needed to be completed before he could approve the HWP. The HP technicians reportedly thought the pre-job survey was one of the steps to be completed before the HWP could be approved. Before the SM approved the entry, he asked the technicians whether they had everything they needed (including the HWP). They responded that they did, thinking that the survey needed to be done to get the HWP approval. The requirements for issuing an HWP include an atmosphere survey for oxygen concentration, a pre-job briefing, extraction gear, and the staging of a back-up extraction team at the access point. All the elements required for the HWP were in place, with the exception of the atmosphere sampling and the pre-job briefing. Because the technicians wore supplied-air respirators, the lack of an atmosphere sample was considered insignificant. No injuries resulted from the event. The WL-101/102 vault, a concrete shell, contains two waste holding tanks. One of the tanks holds intermediate waste water for processing through process equipment waste (PEW) evaporators. The other tank receives the concentrated waste after processing. Potential hazards associated with entry into this vault include nitrous oxide gas, radioactive gases, airborne radioactive contamination and an oxygen deficient atmosphere. The cause of this event was a breakdown in communications between the SM, the Industrial Safety supervisor and the HP Technicians. The involved personnel assumed important information rather than communicating and verifying it. This event illustrates the importance of complete communications, including repeating back essential items. In this case no one was injured because the technicians used the appropriate equipment and back-up personnel were on hand, and no hazard was present at the time. Facilities should use procedures to avoid reliance on memory and assumption, but without adequate communications even the procedures will not always be sufficient to ensure a safe approach to the job. 9. UNAUTHORIZED CRANE MODIFICATION CAUSES NEAR MISS On December 11, 1992, at the Argonne National Laboratory-East Plant Facilities Services (PFS) area, an assembly consisting of a piece of Unistrut and an iron casting weighing approximately seven pounds fell about 15 feet from an overhead 4-ton bridge crane trolley. The assembly missed hitting a plant employee by less than two feet. The assembly had been attached to the overhead crane as a trolley travel stop. It was not part of the original trolley design nor was it an authorized modification of it. Facility personnel stopped the crane and locked it out of service. PFS crane maintenance and safety personnel reconstructed the incident and found that two modifications had been made to the crane. The first modified the power connector follower attached to the bridge. The hoist is the only electrically operated component of this crane. It requires a power cable and connector that must track with the bridge and trolley to provide power to the hoist motor. A chain attaches the connector to the bridge. For unknown reasons the chain had been shortened, thus bringing the connector within the trolley's range of travel. The second modification added the Unistrut and casting assembly that fell from the trolley. This "home made" trolley stop apparently had been installed because the trolley had been contacting the hoist power connector before reaching the manufacturer installed trolley stop, apparently due to the first modification. The crane maintenance group re-located the power connector out of the trolley travel path. The manufacturer installed trolley stop functioned properly with the hoist cable power connector in its correct location. Facility personnel could not determine when the modifications had been made. This event illustrates that unauthorized modifications to facility equipment may cause equipment failures. Facility modification procedures provide a formal method for review, approval and documentation of changes to facility components, systems or structures. Bypassing any of these steps can create hazardous conditions. Review and approval of facility modifications, whether permanent or temporary, should include consideration of potential impacts on facility procedures, training, procurement, maintenance, operations and safety. 10. SEVERE HAND INJURY FROM IMPROPER POWER TOOL MAINTENANCE On January 6, 1993, at Lawrence Livermore National Laboratory, an employee was cleaning and inspecting a rotating grinding wheel and cutting blade when the small and ring fingers of his left hand were severed (ORPS Report SAN--LLNL-LLNL-1993-0001). The employee inadvertently placed his hand in a position where the rotating wheel pulled his fingers into a point where they were pinched with the knife edge. Normal operating practice requires the blade to be backed away from the grinder prior to inspection. There was no written procedure for this task. Also, machine guards did not fully cover the blade/grinding wheel area. The injured employee was transported to a local hospital where both fingers were reattached. Facility personnel locked and tagged the machine out of service, and began a lab wide survey of machine tool guarding. All machine tool equipment should be inspected and evaluated for compliance with OSHA safety standards. Facilities should provide employees engaged in operation and maintenance of machine tools with necessary training and up to date procedures or instructions that address safety hazards. The risk of severe injury may be reduced by establishing various barriers to prevent rotating machine hazardous parts from contacting worker's hands, etc. These barriers usually inspection to ensure compliance with applicable standards, training of operators and maintenance personnel, and written precautions. 11. FIRES AT CHERNOBYL On January 13, 1993, a small fire broke out at the Chernobyl nuclear power station located 80 miles north of Kiev, Ukraine. Ukrainian nuclear officials stated that the fire occurred in a room between the station's first and second reactors and was quickly brought under control. There was no change in radiation levels at the facility. Although the cause of the fire is under investigation, officials speculate that the blaze could have been started after melted snow dripping from the roof caused a short circuit in an auxiliary electrical unit that supplied power to welding equipment. The fire did not affect the two operating reactors at the site. On January 14, 1993, another fire occurred in the ventilation corridor above the cement sarcophagus that covers the Unit No. 4 reactor core. Site personnel quickly extinguished the blaze and no radiation was released. This is the fourth blaze reported at the Chernobyl complex since the April 1986 explosion and fire spread radiation over a wide section of Ukraine and Belarus. Another fire in November 1991 damaged the generator room of reactor No. 1 (Newswire Service). 12. ELECTRICAL FAILURE IN HAWORTH POWERED PANEL On January 4, 1992, in the Drafting Office area at Sandia National Laboratory's Livermore Site, employees heard a breaker trip and simultaneously witnessed a spark, then a flash, from a power connector at the bottom of a Haworth Powered Panel System panel. This system is a room divider with electrical power outlets in the raceway at the base of each panel. The employees found a small scorched area on each side of the panel, and the plastic connector was partially melted (ORPS Report ALO-KO- SNL-LVMRSITE-1993-0001). A similar occurrence was reported in UOR-90-17, dated 5/14/90. These panels have been in service at this site for about ten years. They are designed for a 20-amp load. However, the manufacturer recommends a 16 amp load for extended use. On the morning of January 4, 1993, employees had just returned from holiday. Six employees powered up their work stations, i.e. computers, desk lights, etc. One employee plugged in a 13-amp heater because it was cold in the area. This additional electrical load apparently caused the failure of the panel. One of the most common hazards in the home or the work place is overloading of electrical outlets. (Electrical load in amps can be determined by dividing the device nameplate wattage by the circuit voltage.) In this case, a 1500-watt heater drew about 13 amps (1500 watts divided by 115 volts). In the last decade, increased use of electrical equipment in the work place has challenged the capacity of many electrical circuits. Facility personnel should ensure adequate margins of safety are maintained for partitions containing circuits and electrical outlets, especially if they service work station locations. ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES 1. ADDITIONAL LOCK-OUT/TAG-OUT NONCOMPLIANCES Lock out/Tag out (LO/TO) problems were the subject of recent items in the NS Operating Experience Weekly Summary (Inadequate Interface Between Construction and Operations Tag-outs, NS 92-33; Improper Lock-out/Tag-out Incidents, NS 92-35). Two recent events at Hanford merit this follow-up report. On January 8, 1993, in the Hanford tank farms, a work package was released to perform work related to the installation of an emergency diesel generator at Building 701-A. A LO/TO was approved and installed on day shift except for final verification which was to consist of an independent check of the LO/TO by an operator and a supervisor. Due to a shift change and the fact that the actual work was performed by contractor personnel, the work commenced without the required final verification being done. On December 28, 1992, at the Plutonium Finishing Plant, a LO/TO was installed to assure the de-energizing of a breaker on an electrical panel. Later, the LO/TO Custodian allowed the LO/TO tags to be removed for switch testing by electricians. After testing, the LO/TO tags were re-hung without the required independent verification of the LO/TO. Over the next ten days the LO/TO tags were removed and replaced two more times. In both of these cases managers recognized after the fact that a procedural violation had occurred. In dealing with LO/TO situations, compliance with procedures is MANDATORY to assure personnel safety. Where work extends over several shift crews, and contractor personnel are involved in performing maintenance tasks, communication is vital to ensure that procedural requirements are completed before the work is initiated. 2. FOLLOW-UP ON LITHIUM FIRE IN WASTE HANDLING FACILITY OE Weekly Summary 92-36 reported a lithium fire on December 14, 1992, at the Lawrence Berkeley Laboratory (LBL), as contractor personnel were preparing lithium ribbon for packing. The lithium was being prepared by immersion in methanol inside a fume hood designed for handling hazardous materials. The lithium ignited as it was being immersed in the methanol (ORPS Report SAN--LBL-EHS-1992-0012). Additional information indicates that mineral oil should have been used for immersing the lithium, since methanol is readily miscible with water. The site disposal guide used by contractor employees performing the work merely called for "a solvent" rather than specifying mineral oil. Two additional lessons were learned by the LBL staff from their review of this incident. First, the generator of the waste lacked the training and knowledge to package the lithium correctly, as evidenced by the fact that he had left it in a bag under the fume hood. Had he placed the lithium properly in mineral oil, the contractor personnel responsible for waste disposal would not have had to attempt to immerse it themselves. Second, the contractor personnel should not have attempted to prepare it for disposal without notifying the responsible individual that it had not been packaged correctly. The contractor was a certified waste handler, but his procedure was in error. Vendors have been required to change procedures and retrain their personnel. In addition, LBL staff will now provide strict oversight of vendor staff during the collection, transfer, and packaging of waste. Facilities that routinely handle combustible metals should ensure that employees are trained in extinguishing metal fires. A good reference would be the National Fire Protection Association Standard (NFPA FPH SEC 5-21), "Combustible Metal Extinguishing Agents and Application Techniques." 3. FOLLOW-UP ON DIESEL GENERATOR CYLINDER HEAD PROBLEMS OE Weekly Summary 92-32 discussed problems reported by Gulf States Utilities (GSU) regarding potential problems in Type R-4 diesel generators (DGs) under the manufacturer name Enterprise Engine Company or IMO-DeLaval. Cooper-Bessemer has since acquired IMO-DeLaval and now has the responsibility of notifying owners of the suspect cylinder heads. (NRC EN 24655). Cylinder heads in these DGs cast before August 1, 1984 may have inadequately thick walls. The problem was discovered during an investigation at the River Bend nuclear power plant on October 15, 1992. On that date a diesel generator was taken out of service to investigate traces of engine coolant found in lubricating oil samples. The source of the coolant was identified to be a minute leak from the number four cylinder head into the valve train area, where it drained to the engine base. This event is documented in a 10 CFR Part 21 report (#92-248) to the NRC dated November 16, 1992. On December 17, 1993, Cooper- Bessemer provided further identification of the affected heads to the NRC and owners of their diesel engines. The final report identifies affected heads by serial number and contains recom- mended corrective action. The root cause for the failure at GSU was inadequately thick cast walls at the 3/4"-10 bolt hole indicated on a sketch supplied for the 10 CFR Part 21 notification (Figure 1). Cooper-Besse- mer Design Engineering has reviewed the design drawings to determine whether any other sub-cover bolt holes do not have adequately thick walls between the bolt hole and the adjacent water passage. Their review revealed no other bolt holes with inadequate wall thickness. The affected cylinder heads are identified by one of the following part numbers: 03- 360-03-0F, 1A-6446, 1A-6447, 1A-6879, 1A-6240, 1A-6239, 1A-7062, 1A-5559, 1A-5558, 1A-6266, or 1A-6265, all of which were cast prior to August 1, 1984. Identification of individual heads may be accomplished by referring to Figure 1 and from the following information: All heads have the cast serial number, heat number, cast date, manufacturing date, water test, air test, gas test, and possibly reconditioning information stamped on the head. At Area 1 on Figure 1, which is inside the sub-cover, the serial number, heat number and cast date should be stamped with minimum of ¨" size letters. Area 2 on Figure 1, which is outside the sub-cover on the head, includes serial number, heat number, manufacturing date, water test, air test, gas test information and possibly reconditioning data. Area 1 should be examined for the cast date as stamped by the Enterprise foundry with steel stamps. This may be difficult to see as this area has been painted. Other clues to the age of the cylinder head are at Area 2. If the serial number is L99 or less, and the manufacturing date is before 1986, it is most likely a cylinder head cast prior to August 1, 1984. Any questions concerning cast dates and serial numbers should be directed to John R. Schneider, Manager, Quality Assurance at 412-458-3434. Corrective action includes removing the stud at the location shown in Figure 1 and applying Loctite Hydraulic Sealant (Item No. 56931) or equivalent, per Loctite instru- ctions, to the threaded hole and stud. Tests at Cooper-Bessemer conducted on December 7, 1992, proved this repair sufficient to withstand 100 psi of water pressure (hot or cold) without leakage. Cooper-Bessemer Service Information Memo #384 is being issued which explains this procedure in more detail. This corrective action should be performed at the next scheduled diesel engine outage. Corrective action at Cooper-Bessemer will be to repair this head section on all affected cylinder heads returned to them for rebuilding or repair, using their standard repair EAR-11-001. This involves drilling the hole 1/8" oversize and 1/8" deeper, filling the hole completely with weld metal, redrilling and re-tapping to blueprint size and depth, and re-hydrotesting. Managers of DOE facilities with Type R-4 DGs manufactured by Enterprise Engine Company or their successor, IMO-DeLaval, should determine whether the cylinder heads on their units have this problem, and take appropriate remedial actions. SAFETY NOTICES UNDER DEVELOPMENT: Note: The Office of Nuclear Safety encourages input related to the development of Safety Notices. If you have any questions, comments, or information concerning events or issues similar to those described below, please contact Mr. Ivon Fergus, Office of Nuclear Safety (301) 903-6364. 1. NS has identified a number of events related to the loss of annunciators and other safety-related equipment caused by problems involving 120-VAC/125-VDC systems at DOE and commercial facilities. NS is reviewing potential generic problems associated with the adequacy of 120-VAC/125-VDC systems at DOE facilities. 2. NS evaluated three events associated with the temporary diesel generator at Rocky Flats Plant, Building 707. The lessons learned from these events, particularly as they relate to the control of temporary modifications, are being considered for dissemination in an NS Safety Notice. 3. NS is developing a Safety Notice concerning problems with Uninterruptible Power Supplies (UPS). 4. NS is considering developing a Safety Notice related to control of work at electrical substations and switchyards. 5. NS is developing a Safety Notice related to the handling, storage, venting, and opening of containers and drums that may be pressurized or may contain flammable vapors. This notice will contain generic information about proper storage conditions and the material conditions of containers. 6. NS is working with Lawrence Livermore National Laboratory and DOE-SF personnel to develop a Safety Notice on cracking in ventilation ducting. 7. NS is considering developing a Safety Notice related to Emergency Diesel Generator (EDG) fuel oil supplies. 8. NS is developing a Safety Notice addressing uses of independent verification for equipment positioning. SAFETY NOTICES PREVIOUSLY ISSUED: Safety Notice No. 91-1, "Criticality Safety Moderator Hazards," September 1991 Safety Notice No. 92-1, "Criticality Safety Hazards Associated With Large Vessels," February 1992 Safety Notice No. 92-2, "Radiation Streaming at Hot Cells," August 1992 Safety Notice No. 92-3, "Explosion Hazards of Uranium-Zirconium Alloys," August 1992 Safety Notice No. 92-4, "Facility Logs and Records," September 1992 Safety Notice No. 92-5, "Discharge of Fire Water Into a Critical Mass Lab," October 1992 Safety Notice No. 92-6, "Estimated Critical Positions (ECPs)," November 1992 Copies of NS Safety Notices may be requested from: Nuclear Safety Information Center, Office of Nuclear Safety, U.S. Department of Energy, Room S161, GTN, Washington, DC 20585