LAX84LA050
NTSB Identification: LAX84LA050 .
The docket is stored on NTSB microfiche number 22808.
Accident occurred Sunday, November 06, 1983 in SAN JOSE, CA
Aircraft: CESSNA 150H, registration: N23268
Injuries: 2 Minor.

THE ACFT WAS FLOWN FROM SAN JOSE, CA TO AN ARPT NEAR SUTTER CREEK, CA WHERE THE PLT LANDED. BEFORE TAKING OFF ON THE RETURN FLT, HE VISUALLY CHECKED THE FUEL, AND ACCORDING TO HIM, THE FUEL WAS WITHIN 1/2 INCH FROM THE TOP OF THE TANKS. NO FUEL WAS ADDED BEFORE DEPARTING. DURING ARRIVAL AT SAN JOSE, THE ENG LOST POWER, ABOUT 2 1/4 MI FROM THE DESTINATION ARPT, AND WOULD NOT RESTART. AT THAT TIME, THE PLT NOTICED THAT THE LEFT FUEL GAGE INDICATED NEARLY 1/4 FULL & THE RIGHT GAGE INDICATED 1/8 FULL. DURING A FORCED LANDING, THE ACFT HIT A BERM & WAS DAMAGED. AN EXAM OF THE FUEL TANKS REVEALED THERE WAS LESS THAN 3 GAL OF FUEL REMAINING. THE FUEL CAPACITY OF THE PLANE WAS 26 GAL, OF WHICH, 22.5 GAL WAS CONSIDERED AS USABLE. THE ACFT HAD FLOWN 4 HRS SINCE IT WAS REFUELED. ACCORDING TO THE OWNER'S MANUAL, THE PLANE'S ENDURANCE AT 4000 FT WITH 75% POWER WAS 4 HRS. ALSO, THE MANUAL STATED THAT THIS VALUE COULD VARY 10% OR MORE DUE TO VARIABLES SUCH AS CARB METERING CHARACTERISTICS, ENG & PROP CONDITION, & ATMOSPHERIC CONDITIONS.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

PREFLIGHT PLANNING/PREPARATION..INADEQUATE..PILOT IN COMMAND
FUEL SUPPLY..MISJUDGED..PILOT IN COMMAND
FLUID,FUEL..STARVATION
FUEL SUPPLY..INADEQUATE..PILOT IN COMMAND


Contributing Factors

TERRAIN CONDITION..DIRT BANK/RISING EMBANKMENT
ENGINE INSTRUMENTS,FUEL QUANTITY GAGE..FALSE INDICATION

Index for Nov1983 | Index of months