NS OPERATING EXPERIENCE WEEKLY SUMMARY 93-5 January 29 - February 4, 1993 The purpose of the NS Operating Experience (OE) Weekly Summary is to enhance safety throughout the DOE complex by promoting the feedback of operating experience and by encouraging the exchange of information among DOE nuclear facilities. The OE Weekly Summary is distributed for information only. No specific actions or responses are required solely as a result of this document. Readers are cautioned that review of the OE Weekly Summary should not be relied upon as a substitute for a thorough review of the interim and final Occurrence Reports. The following events were reviewed during the week of January 29 - February 4, 1993. ITEM PAGE 1. FACILITY OPERATIONS AFFECTED BY OUT-OF-POSITION VALVES 1 2. PUMP BOLTING DEFICIENCIES 2 3. STANDBY AIR COMPRESSOR FAILURES AT SAVANNAH RIVER K-REACTOR 3 4. WATER HAMMER CAUSES STEAM LEAK AT SAVANNAH RIVER H-CANYON 4 5. OCONEE REACTOR TRIP AND SUBSEQUENT SWITCH MISPOSITIONING 4 6. CONTAMINATION AND POTENTIAL PERSONNEL EXPOSURE AT TANK FARM 5 7. LESS THAN ADEQUATE PROCEDURE REVIEW CAUSES VENTILATION PROBLEM 6 8. EXPLOSION OCCURS IN LABORATORY FURNACE 6 9. FATAL ACCIDENT IN SUPERCOLLIDER TUNNEL 7 10. EMERGENCY DIESEL GENERATOR FAILURE CAUSED BY PAINTING 8 11. SUBSTANDARD BREAKERS IDENTIFIED AT Y-12 8 12. BATTERY PREVENTIVE MAINTENANCE (PM) 9 ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES 1. FAILURE OF VICTAULIC CAP DURING PRESSURE TEST 10 1. FACILITY OPERATIONS AFFECTED BY OUT-OF-POSITION VALVES NS reviewed three occurrences this week in which out-of-position valves affected facility operations. On February 1, 1993, personnel evacuated a building at the Pantex Plant when an out-of-position valve created the danger that a fire suppression deluge could have been inadvertently activated. Construction personnel were releasing air pressure after testing a new air compressor system. However, a valve thought to be closed was open, allowing plant system air to be released along with air from the construction air system. The resulting low pressure into the plant air system required personnel to block the fire suppression deluge system, and the affected building was evacuated due to Limiting Conditions of Operation (LCO) requirements. Facility personnel have not been able to determine when the valve was opened. Facility personnel blocked closed the subject valve, along with six other valves that if opened could affect plant operations (ORPS Report ALO-AO-MHSM-PANTEX-1993-0007). On January 31, 1993, a sample pump seal at the Savannah River Defense Waste Processing Facility was damaged when it was operated for several minutes without seal water flow. The seal water isolation valve for that type of seal was normally left open, but facility personnel closed the valves after experiencing problems with excessive leakage. However, procedures were not updated to include a requirement to open the seal water isolation valve before starting the pump. As a result, operators started the pump and ran it for several minutes without seal water flow, damaging the seal. Facility personnel have identified and corrected all affected procedures (ORPS Report SR--WSRC-WVIT-1993-0002). On January 28, 1993, a uranium enrichment production cell at the Portsmouth Gaseous Diffusion Plant automatically shut down when operators inadvertently activated a compressor motor oil pressure sensor. Operators closed a lube oil supply valve to the compressor motor in order to replace a leaking oiler. The lube oil lines for some stages contain oil pressure sensors, while others do not. Closing this valve while the motor is running is normal practice for stages without oil pressure sensors, since the oiler can be replaced in about one minute and motor bearing heatup is not significant. However, the oil line for this stage contained a pressure sensor, which sensed the low oil pressure condition and activated the motor trip circuit, shutting down the motor and the associated cell. Had the operators verified that this stage contained an oil pressure sensor, they would have performed a planned cell shutdown to replace the oiler (ORPS Report ORO--MMES-PORTCASOPS-1993-0003). In each of these occurrences, correct valve positions were not verified by positive means. These events underscore the importance of using positive means, including independent verification, to verify the position of all valves that could affect the performance of a test or maintenance activity. Even those valves not normally operated and expected to be in a normal position should be verified if their position could adversely affect plant operation or personnel safety. The Savannah River event also illustrates the need for facility personnel to ensure that they adequately control abnormal valve alignments including documentation of restoration to normal alignment. For safety-related applications, this should include independent verification of the restoration. Also, the Pantex occurrence emphasizes the importance of communications between construction and operations personnel when operating equipment that provides boundaries between construction and plant activities. 2. PUMP BOLTING DEFICIENCIES On January 29, 1993, personnel at the Advanced Test Reactor (ATR) in Idaho discovered that the M-6 coolant pump in the 1C-W experiment loop was mounted with only two bolts, instead of the required four bolts. Four horizontally mounted coolant pumps pump water through the 1C-W loop, which is one of nine ATR experiment loops. Facility personnel inspected the other pumps in the loop and identified another mounted with only three bolts. Workers, using a recently updated procedure, were performing maintenance on one of the affected pumps when they discovered the deficiency. Previous revisions of the pump replacement procedure included multiple actions within procedure steps. In the latest revision of the procedure, multiple action steps were divided making it clearer and easier for the craft personnel to use. Workers stopped the maintenance when they were unable to perform the step requiring that four bolts be inserted because of an alignment problem. The 1C-W M-6 pump had been repaired in May 1992, and facility personnel have not been able to determine how long the condition existed. Proper bolting of the coolant pumps is a concern because catastrophic failure of the pumps or loop piping could cause the Experiment Loop to void, which adds positive reactivity to the ATR core. Engineering personnel have performed analysis indicating that the bolting deficiency would not have increased the probability or the consequences of any previously analyzed accidents and therefore did not result in an Unreviewed Safety Question (USQ). In this event, use of detailed procedures and good maintenance practices by craft personnel led to the discovery of a condition that had gone undetected. This event illustrates the benefits of using detailed procedures and underscores the need for craft personnel to inform facility management when deficiencies are noted. This is especially important because craft personnel may not be aware of facility safety analysis and design basis requirements, and should not be expected to make decisions as to the adequacy of deficiencies. To address these concerns, ATR personnel are discussing this issue with all craft personnel and are continuing to upgrade maintenance procedures (ORPS Report ID--EGG-ATR-1993-0004). 3. STANDBY AIR COMPRESSOR FAILURES AT SAVANNAH RIVER K-REACTOR On January 31, 1993, at the Savannah River Site K-Reactor, Central Control Room operators received the 'Standby Air Low Pressure' annunciator. An operator, investigating the condition, found that the A compressor coupling had failed and the redundant B compressor had started. The operator then discovered that a solenoid valve was stuck open on the B compressor, preventing it from maintaining system pressure. The operator tapped on the solenoid valve causing it to close and restore pressure to normal. The operator then stopped the A compressor motor. System pressure did not decrease sufficiently to cause any dampers in the confinement system to change position (ORPS Report SR--WSRC-REACK-1993-0017). This pair of low capacity air compressors supply control air to dampers in the facility confinement system. They are included in the facility preventive maintenance and surveillance programs. The facility operators increased the monitoring frequency on the B compressor as a compensatory action during this degraded condition and initiated work requests to have both compressors repaired. Establishing compensatory action on equipment in a degraded condition is a good practice. Preventive maintenance and surveillance programs do not guarantee that equipment will always function as required nor do redundant components always protect against single failures. Predictive maintenance tracking systems can be used to identify the frequency of failure of components and allow fine tuning of preventive maintenance schedules and replacement part inventories. 4. WATER HAMMER CAUSES STEAM LEAK AT SAVANNAH RIVER H-CANYON On January 31, 1993, personnel at the Savannah River H-Canyon facility discovered a steam leak in the branch header that supplies main steam to process vessels and building heating. While placing the system into service, operations personnel heard a load noise and identified a 14-inch steam isolation valve gasket leaking steam. Facility personnel immediately initiated an emergency shutdown of the system (ORPS Report SR--WSRC-HCAN-1993-0012). They conducted a walkdown of the steam system and reported that this event caused no personnel injury or process disturbances. (All processes had been shut down for the steam system outage.) Facility personnel report that the leak occurred because of a water hammer that began when the system was valved into service. They suspect that the system was brought on-line too fast, and proper pre-heat of the piping was not provided. Introduction of hot water or steam into colder piping can result in water hammer, piping deflection and hanger damage. The procedure used for system start-up did not provide specific time intervals for warming the system before introducing steam. Facility personnel are now committed to revise the system start-up procedure to provide these intervals. This event emphasizes the importance of ensuring system temperature and equilibrium pressure when valving systems into service. Water hammer and thermal stresses in piping systems has been the subject of numerous commercial nuclear industry events. Additional information concerning this subject can be found in NRC Information Notices IN 91-38 "Thermal Stratification in Feedwater System Piping"; IN 88-80 "Unexpected Piping Movement Attributed to Thermal Stratification"; IN 89- 90 "Potential for Water Hammer, Thermal Stratification, and Steam Binding in HPCI Systems"; NRC Bulletin NRCB 88-08 "Thermal Stresses in Piping Connected to Reactor Coolant Systems"; NRCB 88-11 "Pressurizer Surge Line Thermal Stratification"; and the Institute of Nuclear Power Operations (INPO) SER 25-87 "Pressurizer Surge Line Thermal Cycling." 5. OCONEE REACTOR TRIP AND SUBSEQUENT SWITCH MISPOSITIONING On January 26, 1993, a technician at the Oconee Unit 3 nuclear power plant caused two fuses to blow in a circuit supplying the main generator electrical output signal to the plant's Integrated Control System (ICS). The ICS processes steam flow, feedwater flow, feedwater pump discharge pressure, generator load, average reactant coolant temperature, and other parameter signals to automatically control steady state and transient plant load demands. Because of the blow fuses, the indicated main generator electrical output decreased below the demand value on the ICS. The ICS then opened the main turbine valves further in an attempt to return the generator electrical output to the ICS demand value. This increased steam flow to the main turbine and caused the main feedwater pump discharge pressure to decrease. The main turbine then tripped because of the low feedwater discharge pressure and the Reactor Protection System (RPS) automatically tripped the reactor as a result of the turbine trip. The plant responded normally after this full power reactor trip with the Emergency Feedwater System (EFW) actuating as expected (NRC EN 24947). Plant investigators believe the technician incorrectly positioned the selector switch on the multi-meter he was using to troubleshoot the equipment, causing the fuses to blow. Plant personnel have not finalized all corrective actions. Potential corrective actions include, changing the color of the indicating lights to make them more noticeable, evaluating middle-of-shift operator relief practices, determining if the use of check offs in AOPs should be mandatory, and verifying the adequacy of the training for technicians who use multi-meters. About two hours after the reactor trip, a second problem occurred. The operators restarted the Main Feedwater (MFW) System and then shutdown the EFW system in accordance with the Abnormal Operating Procedure (AOP) for Loss of MFW. The licensed operator who performed the AOP, did not correctly position two EFW system control valve switches in the "manual" versus "automatic" position as required by the AOP and the plant technical specifications. The operators sometimes use a check mark to note the steps accomplished in an AOP. The use of AOP check offs is considered optional and this operator did not use it. The status of these valves is indicated by two white lights, one labeled "Manual" the other "Automatic." The EFW system was incapable of automatically providing EFW flow to the SGs when these switches were in manual. This operator was relieved by another operator later during the shift (not a normal shift turnover). These two operators did not adequately review the control boards and the mispositioned switches were not discovered. Operators discovered the mispositioned switches during a control board walk-down for formal shift turnover, about five and one-half hours later. This event demonstrates how casual operating practices (optional use of check offs, informal shift relief) can result in the failure to meet operating requirements. Facilities can prevent the occurrence of similar events by maintaining compliance with the requirements of Conduct of Operations manuals and other facility procedures. 6. CONTAMINATION AND POTENTIAL PERSONNEL EXPOSURE AT TANK FARM On January 21, 1993, at the 241-SY Tank Farm at Hanford, operators found indication of a leak of contaminated liquid from a waste storage tank. Plant personnel estimated that about 8 oz. of contaminated liquid had leaked onto the snow and soil. The operators had been preparing to move an overpack (a large pipe sealed at both ends) containing an air lance when they discovered the leak. Three air lances had been removed from Tank TK-101-SY and stored at this location in overpacks. Tank TK-101-SY is a one-million-gallon tank that is at the top of the tank watch list for the Hanford Site. Operators had used the air lances in the past to mix the waste stored in the tank. The highest radiation reading from the leaking overpack was 80 mR/hr. The spill was cleaned up, and the contaminated material was properly disposed of (ORPS Report RL--WHC-TANKFARM-1993-0010). The air lances are no longer in use. Investigators determined that after placing the air lance into its receiver, operators covered the four inch drain in the over pack with plastic sheeting and tape. During the subsequent inclement weather, snow and ice accumulated on the air lance; when the ice melted, it carried contamination into the overpack. The plastic sheeting then failed, and the contaminated liquid leaked to the soil. In retrospect, site engineers indicated, a blank flange would have been a better choice for sealing the four-inch opening. Later the same day, at the same Hanford location, four workers in a "greenhouse," a temporary containment structure, noted a strong ammonia odor as they attempted to install a drain line on an overpack assembly for an air lance. All were wearing respiratory protection masks. They noted the odor when they removed a one-inch pipe plug. One worker left the area, complaining of burning eyes, sore throat, and a headache. After examination, he was returned to the work site. Upon his return, they all switched to supplied breathing air respirators and finished the installation. The next day industrial hygiene personnel checked the work site and found air-borne contamination in the air lance receivers. Health Physics staff were still working to establish the levels of radiation exposure experienced by the four workers. This investigation is continuing, but site personnel have determined that the flushing procedure used to decontaminate the overpacks and air lances was inadequate. Had the overpacks and air lances been treated as potential mixed waste, the incident could have been avoided. Staff have added a visual inspection and radiation survey to the standard flush procedure to ensure that no "crud" remains on equipment that has been inside a high level waste tank. Facilities dealing with high level waste should make sure that the job planning process includes every possible safety precaution to avoid contamination or personnel exposure. Equipment that has been used inside a tank holding high-level wastes should be treated as radiologically and chemically unsafe until properly surveyed by trained personnel. 7. LESS THAN ADEQUATE PROCEDURE REVIEW CAUSES VENTILATION PROBLEM On January 25, 1993, at Rocky Flats Building 561, an operator caused the Process Air Programmer (PAP) to cycle while performing a post maintenance test (PMT) on a fan in the ventilation system. The PMT required the standby fan to be energized, but the operator did not identify the correct HAND-OFF-AUTO fan switch position. Cycling the PAP shut off the ventilation to the building, but the exhaust fan for affected gloveboxes remained in operation. No plutonium operations were underway at the time of this occurrence. Facility personnel verified that the PAP cycled in proper sequence and returned the ventilation system to normal (ORPS Report RFO--EGGR- ANALYTOPS-1993-0007). The inadequacy of the procedure was identified in a procedure change notice in October 1991. The PMT has been performed successfully during the interim period by using experienced operators knowledgeable of the procedure problem. After the engineering review process, a Procedure Revision Request (PRR) was issued in June 1992. The PRR is currently waiting approval from the Validation and Verification group but higher priority work has slowed the process. In this event, 15 months had elapsed between identification of a problem and issuance of a notification report. Facility personnel need to address procedure deficiencies with formal changes rather than relying on operator experience to work around the deficiencies. An important safety issue, such as proper glovebox or building ventilation, should receive prompt attention. 8. EXPLOSION OCCURS IN LABORATORY FURNACE On January 29, 1993, a worker at the Oak Ridge Analytical Chemistry Laboratory discovered a furnace in Building 4500-S damaged by an apparent explosive chemical reaction. No personnel were injured as a result of the explosion and the damage was confined to the furnace. Health Physics personnel surveyed the furnace and found no contamination (ORPS Report ORO--MMES- X10ANLCHEM-1993-0002). The damaged furnace is the size of a small microwave oven and is located under a laboratory hood. Personnel use the furnace to oxidize or "ash" the samples. Prior to the event, laboratory personnel had placed four beakers in the furnace, each containing approximately 10 grams of residue. This residue was particlate material collected from the off-gas stack. Environmental personnel used stainless steel probes in the stack to collect the particulate samples before sending the samples to the laboratory for radionuclide analysis. They used a stack probe wash procedure to collect the residue from the probe in 250 ml aliquots. The sample was then taken to the laboratory and heated to dryness in the furnace before conducting the radionuclide analysis. Environmental personnel had discussed the probe washing procedure with the laboratory group supervisor who suggested that the probes be cleaned using a 4M nitric acid solution. Environmental personnel decided to use a commercially available solution named "Radiac Wash" to clean the probes instead of the previously agreed upon nitric acid, and did not inform the laboratory group leader of the change. When samples of the probe washing were submitted for further processing, the material description on the request form stated "WATER & RADIAC WASH." Laboratory personnel assumed that "Radiac Wash" was the name given to the probe wash procedure and that the solution was the 4M nitric acid, as had been previously discussed. During processing, a laboratory technician noticed what appeared to be organic contaminates in the sample. A decision was made to ash the sample, a normal procedure when organics are present. The pH of the aliquot was adjusted using nitric acid and placed into the furnace. The furnace heats the sample 100 degrees Centigrade every 100 minutes until a maximum temperature of 500 degrees is attained. The temperature of the oven was at 200 degrees when the violent reaction occurred. After the event, laboratory personnel determined that "Radiac Wash" contained several organic constituents, some of which form explosive compounds in the presence of nitric acid (e.g., ethylene oxide). This event underscores the importance of having properly qualified personnel conduct a hazards evaluation when using new chemicals. The Radiac Wash had not been analyzed for possible volatile reactions with other chemicals used in the process. An effective hazards analysis and chemical control program would have required the analysis of all chemicals and their applications prior to use and could have assisted in preventing this event. 9. FATAL ACCIDENT IN SUPERCOLLIDER TUNNEL On January 29, 1993, in the Super-Conducting Supercollider tunnel, a 6000 lb. segment of concrete tunnel liner fell, killing a construction worker at the N-15 construction site. Construction management suspended all operations until the cause of the accident is determined (Ref. ORPS Report HQ--URA-SSCL-1993-0001). The concrete segment is about 5 feet wide by 8 feet long and 9 inches thick and is one of four segments used to line each 8-foot section of the 2.7-mile tunnel section presently under construction. Construction workers positioned the segment, using hydraulic jacking equipment, and then installed hydraulic supports to hold it in place. It is believed that one of these hydraulic supports retracted, allowing the segment to fall. DOE is conducting an investigation of the accident, and Parsons- Brinkeroff/Morrison-Knudsen, the architect/engineer/construction firm managing the tunnel construction, is performing its own investigation in parallel. A followup report will be included in the weekly summary as information becomes available. 10. EMERGENCY DIESEL GENERATOR FAILURE CAUSED BY PAINTING On January 21, 1993, personnel at the South Texas Project commercial nuclear power plant informed the NRC that one of their emergency diesel generators (EDGs) had been inadvertently rendered inoperable when it was painted. During a subsequent surveillance test, the EDG failed to start. Personnel painted the EDG as part of an upgrade to plant appearance and housekeeping. This was the first diesel to be painted. The plant decided to paint the diesel without taking it out of service (OOS) to avoid operating penalties if the diesel was OOS for more than 72 hours. This decision permitted deleting the post-maintenance test of the diesel because it had not been taken OOS. Paint dripped into the metering rod guide holes in the "jerk pumps" (impulse injection pump) and caused the lockup. Plant personnel removed the paint from the rod guide holes, verified free movement of the metering rods, and successfully started the diesel (NRC EN 24914). The Institute of Nuclear Power Operations (INPO) reported paint binding problems at three commercial nuclear power plants - McGuire 1, Byron 1, and Palo Verde 3 (INPO Safety Evaluation Report 16-90). Corrective actions stated in the INPO document include: (1) a thorough pre-job briefing for the painters, (2) operational tests to verify equipment reliability after painting, and, (3) restrictions on redundant components so that operational testing is completed on one redundant component prior to the next one being painted. This INPO SER was available at South Texas but its recommendations were not followed. NRC Information Notice 90-80, Sand Intrusion Resulting in Two Diesel Generators Becoming Inoperable, dated December 21, 1990, discusses a similar problem. This notice also describes a case where personnel cleaned the DG intercoolers and treated them with a corrosion-preventive agent. The intercoolers had been removed from the diesel engine and prepared for sandblasting by bolting plywood covers over the shell side and sealing the wood with tape. The covering did not seal adequately and aluminum oxide entered the shell side of the intercoolers. During subsequent DG operation, sand was deposited between the piston rings and cylinder liners, causing heavy scoring. Awareness of the vulnerability of diesels to ingestion of foreign material can help avoid unnecessary DG down time. Combustion air intakes must be protected to prevent the entry of debris. Externally exposed moving parts must be protected from paint, cleaning solutions, etc. to maintain operability. Strict cleanliness practices and post-maintenance inspections must be enforced to maintain equipment reliability. 11. SUBSTANDARD BREAKERS IDENTIFIED AT Y-12 On January 27 and 28, 1993, facility personnel at the Oak Ridge Y-12 Site identified two General Electric breakers as suspect equipment while performing inventory activities. Upon close inspection, warehouse personnel discovered various non- conforming conditions including missing factory seals, RTV used to plug ports in the casing, grind marks on the casing, and inadequate shipping containers. These breakers were not consistent with the shipping and material quality standards specified by site personnel. The suspect breakers are 120-volt, 3 phase with serial number TQD-32150 and manufactured in Brazil (ORPS Reports ORO--MKFO-Y12CENTENG- 1993-0004 and ORO--MKFO- Y12CENTENG-1993-0005). This event demonstrates the importance of implementing a program to inspect equipment upon receipt from the vendor. Quality Assurance programs and procedures are effective in identifying suspect materials. Facilities may want to notify their Quality Assurance department of this potential problem. Substandard, counterfeit, and other suspect parts used in nuclear applications is a concern for both Government contractors and the commercial nuclear industry. The use of suspect materials in critical applications poses a threat to DOE facility operation and nuclear safety and may present plant workers, the public and the environment with increased risk. The Inspector General issued a report in September 1990 concerning the Department's Quality Assurance processes relative to this issue. As a result of this report, the Program Secretarial Officers initiated a program to identify suspect parts and initiate corrective actions. Additional information concerning programs that the Nuclear Regulatory Commission consider to be effective in providing the capability to detect counterfeit or fraudulently marked products and assure the quality of procured products may be found in NRC Generic Letter 89-02 "Actions to Improve the Detection of Counterfeit and Fraudulently Marketed Products." This document lists numerous NRC Bulletins and Information Notices concerning nonconforming materials and equipment and instances of inadequate dedication of equipment for safety-related applications. 12. BATTERY PREVENTIVE MAINTENANCE (PM) On October 7, 1992, the NRC issued a supplement to Information Notice 91-64, Site Area Emergency Resulting from a Loss of Non-Class 1E Uninterruptible Power Supplies. Information Notice 91-64 was originally issued in response to the August 13, 1991, event at Nine Mile Point Unit 2 nuclear power plant. During that event, a voltage disturbance on the electrical distribution buses, the facility lost power from each of five Non-Class 1E Uninterruptible Power Supplies (UPS). The NRC supplement provided additional information on replacement intervals for control logic back-up power battery packs associated with Exide Electronics, Incorporated (Exide) 75 KVA UPS model No. 575-60T3-120/208. The Exide UPS units have internal continuously charged back-up batteries to prevent a loss of control logic power. Exide's UPS control logic circuitry receives, processes, generates, and sends electrical signals essential for proper UPS operation. However, at Nine Mile Point, the back-up power battery packs were apparently past their useful life and were completely discharged. The loss of power from the UPSs caused the loss of a number of critical instrumentation and control systems at the plant. Exide used Gates Energy Products (Gates) rechargeable batteries for its UPS control logic batteries. The NRC investigation of the event determined that functional battery packs acting alone would support the amperage consumption necessary for the UPS control logic to operate for at least 10 minutes. The Gates performance data sheets show that battery life expectancy is a function of float voltage and temperature with charge and discharge cycle life being a function of the depth of discharge. The Gates data also show that greater float voltage or higher operating temperatures decrease battery life. For example, a battery could last slightly longer than five years with an operating temperature of 30 ¯C and a float voltage of 2.3 volts DC (vdc). If the operating temperature is increased to 40 ¯C with a float voltage value of 2.3 vdc, the battery life expectancy is about three years. If the float voltage is increased to 2.4 vdc, the life expectancy is about two years. Further, if the operating temperature is increased to 50 ¯C and the float voltage is 2.4 vdc, the battery life expectancy decreases to about one year. Therefore, high float voltage combined with excessively high operating temperature substantially decrease battery life. At Nine Mile Point, the UPS back-up internal battery packs were completely discharged, and the utility had not performed adequate PM on the battery packs commensurate with the actual in-service conditions that could adversely affect battery life. The lessons learned at Nine Mile Point are applicable to a number of DOE facilities. Installations with UPSs that contain backup batteries should assure the batteries receive periodic PM and are operated within the manufacturer's life expectancy temperature and float voltage requirements. ADDITIONAL INFORMATION RELATED TO FOLLOWUP ACTIVITIES Correction: In OE Weekly Summary 92-36, NS described a lithium fire at the Lawrence Berkeley Laboratory waste handling facility. The event description stated that lithium is a strong oxidizer and reacts with water to form hydrogen. In fact, lithium is incompatible with strong oxidizers. 1. FAILURE OF VICTAULIC CAP DURING PRESSURE TEST In OE Weekly Summary 93-1, NS reported an event in which a Victaulic cap failed during an air pressure test at the Morgantown Energy Technology Center (METC) in West Virginia, causing minor damage to the facility. Workers were using the Victaulic cap to establish a pressure boundary at the end of an 8 main fire header. Not relying completely on the clamping bolts, facility personnel had wedged a 4 X4 post against the cap to help prevent it from blowing off. While the line was pressurized with 120 psig air, the post slipped off and the cap loosened and blew off. Mud, stone and water were blown onto the side of a building, breaking the outer panes of two 30 X36 windows (ORPS Report HQ--GOME-METC-1993-0002). In OE Weekly Summary 93-1, NS mentioned lessons learned from this event concerning work package review and proper restraint of temporary devices. However, personnel at other facilities have provided feedback to NS pointing out additional lessons to be learned from this event. They point out that this event illustrates that pressure tests should be conducted with water, and air tests should only be performed where special circumstances preclude the use of water. The use of water minimizes the amount of energy that would be released if the system under test fails, since water is essentially incompressible. Had a hydrostatic test been performed on this system, instead of the air test, debris would not have been blown into the building and no damage would have resulted. However, if special circumstances dictate that a system be pressure tested with air, special precautions should be taken to ensure that all temporary components are adequately restrained. Generally, temporary piping components must meet the same design and installation criteria as the permanent system. Commercial piping design codes also contain general guidance for circumstances in which an air test versus a hydrostatic test may be used. This event also demonstrates the importance of keeping non-essential personnel clear of areas where air tests are being conducted. SAFETY NOTICES UNDER DEVELOPMENT: Note: The Office of Nuclear Safety encourages input related to the development of Safety Notices. If you have any questions, comments, or information concerning events or issues similar to those described below, please contact Mr. Ivon Fergus, Office of Nuclear Safety (301) 903-6364. 1. NS has identified a number of events related to the loss of annunciators and other safety-related equipment caused by problems involving 120-VAC/125-VDC systems at DOE and commercial facilities. NS is reviewing potential generic problems associated with the adequacy of 120-VAC/125-VDC systems at DOE facilities. 2. NS evaluated three events associated with the temporary diesel generator at Rocky Flats Plant, Building 707. The lessons learned from these events, particularly as they relate to the control of temporary modifications, are being considered for dissemination in an NS Safety Notice. 3. NS is developing a Safety Notice concerning problems with Uninterruptible Power Supplies (UPS). 4. NS is considering developing a Safety Notice related to control of work at electrical substations and switchyards. 5. NS is developing a Safety Notice related to the handling, storage, venting, and opening of containers and drums that may be pressurized or may contain flammable vapors. This notice will contain generic information about proper storage conditions and the material conditions of containers. 6. NS is working with Lawrence Livermore National Laboratory and DOE-SF personnel to develop a Safety Notice on cracking in ventilation ducting. 7. NS is considering developing a Safety Notice related to Emergency Diesel Generator (EDG) fuel oil supplies. 8. NS is developing a Safety Notice addressing uses of independent verification for equipment positioning. SAFETY NOTICES PREVIOUSLY ISSUED: Safety Notice No. 91-1, "Criticality Safety Moderator Hazards," September 1991 Safety Notice No. 92-1, "Criticality Safety Hazards Associated With Large Vessels," February 1992 Safety Notice No. 92-2, "Radiation Streaming at Hot Cells," August 1992 Safety Notice No. 92-3, "Explosion Hazards of Uranium-Zirconium Alloys," August 1992 Safety Notice No. 92-4, "Facility Logs and Records," September 1992 Safety Notice No. 92-5, "Discharge of Fire Water Into a Critical Mass Lab," October 1992 Safety Notice No. 92-6, "Estimated Critical Positions (ECPs)," November 1992 Copies of NS Safety Notices may be requested from: Nuclear Safety Information Center, Office of Nuclear Safety, U.S. Department of Energy, Room S161, GTN, Washington, DC 20585