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Event Notification Report for May 13, 2003




                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           05/12/2003 - 05/13/2003

                              ** EVENT NUMBERS **

39838  39840  39841  39842  

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39838       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUMMER                   REGION:  2  |NOTIFICATION DATE: 05/12/2003|
|    UNIT:  [1] [] []                 STATE:  SC |NOTIFICATION TIME: 03:28[EDT]|
|   RXTYPE: [1] W-3-LP                           |EVENT DATE:        05/12/2003|
+------------------------------------------------+EVENT TIME:        01:02[EDT]|
| NRC NOTIFIED BY:  EDDIE BYARS                  |LAST UPDATE DATE:  05/12/2003|
|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |PAUL FREDRICKSON     R2      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       100      Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC TURBINE TRIP/REACTOR TRIP DUE TO MAIN GENERATOR OUTPUT BREAKER     |
| OPENING                                                                      |
|                                                                              |
| Main Generator output breaker opened after receiving Main Generator voltage  |
| regulator # 1 (core 1)  & # 2 (core 2) alarms causing an automatic turbine   |
| trip followed by an automatic reactor trip  (first out annunciator was over  |
| temperature differential temperature).  All rods fully inserted into the     |
| core.  Both motor driven auxiliary feedwater pumps were manually started to  |
| maintain reactor coolant temperature and proper steam generator water        |
| levels.  Steam is being dumped to the main condenser.  Emergency Operating   |
| procedure 1.0 entered and then Emergency Operating procedure 1.1, Reactor    |
| Recovery Procedure was entered.   All emergency core cooling systems and the |
| emergency diesel generators are fully operable if needed.  The licensee      |
| believes that the main generator exciter breaker opened before the main      |
| generator output breaker opened. No work was going on in the area of the     |
| main generator when the output breaker opened.                               |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   39840       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  STATE OF MISSOURI                    |NOTIFICATION DATE: 05/12/2003|
|LICENSEE:  MISSOURI  DEPT. OF TRANSPORTATION    |NOTIFICATION TIME: 14:57[EDT]|
|    CITY:  JEFFERSON CITY           REGION:  3  |EVENT DATE:        05/10/2003|
|  COUNTY:  COLE                      STATE:  MO |EVENT TIME:        18:00[CDT]|
|LICENSE#:  24-20415-01           AGREEMENT:  N  |LAST UPDATE DATE:  05/12/2003|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |SONIA BURGESS        R3      |
|                                                |FRED BROWN           NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  BETH BROWN                   |                             |
|  HQ OPS OFFICER:  HOWIE CROUCH                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|BLO1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOST AND THEN RECOVERED TROXLER ASPHALT CONTENT GAUGE                        |
|                                                                              |
| The following information was obtained from the licensee via facsimile:      |
|                                                                              |
| "On Saturday evening, May 10, 2003, at approximately 6:00 pm [CDT], a        |
| tornado wiped out a trailer at an asphalt plant that contained an asphalt    |
| nuclear gauge 3241 [Troxler]. The gauge was in its gray shipping container   |
| that was locked inside a metal case, which was bolted to the floor. The      |
| gauge was found about 100 feet from the trailer site out of the metal box,   |
| but the gray shipping case was still intact. It did not appear to be         |
| damaged. The contractor, Chester Bross Construction Company, found the gauge |
| and stored it in their plant shack with their gauge. Their Safety Director,  |
| [DELETED], also came up on Sunday morning and took readings. Neither gauge   |
| appeared to be leaking."                                                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Hospital                                         |Event Number:   39841       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  TRIPLER ARMY MEDICAL CENTER          |NOTIFICATION DATE: 05/12/2003|
|LICENSEE:  TRIPLER ARMY MEDICAL CENTER          |NOTIFICATION TIME: 17:32[EDT]|
|    CITY:  HONOLULU                 REGION:  4  |EVENT DATE:        05/12/2003|
|  COUNTY:                            STATE:  HI |EVENT TIME:        11:00[HST]|
|LICENSE#:  53-00458-04           AGREEMENT:  N  |LAST UPDATE DATE:  05/12/2003|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |LINDA SMITH          R4      |
|                                                |SONIA BURGESS        R3      |
+------------------------------------------------+MELVYN LEACH         NMSS    |
| NRC NOTIFIED BY:  MAJ. ARTHUR MORTON, USA      |MATT HAHN            IAT     |
|  HQ OPS OFFICER:  HOWIE CROUCH                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|BLO1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NUCLEAR MATERIAL MISSING DURING SHIPMENT                                     |
|                                                                              |
|                                                                              |
| The following information was received from the licensee via facsimile:      |
|                                                                              |
| "An order for 150 milli-curies (mCi) of iodine-131 was placed with           |
| Mallinckrodt on May 9, 2003. The package was received by the Nuclear         |
| Pharmacist,[DELETED], on May 12, 2003 and indicated that the package had     |
| 154.10 mCi of iodine-131 but was measured to contain only 54.0 mCi of        |
| iodine-131.                                                                  |
|                                                                              |
| "At 11:00 [HST] the Nuclear Pharmacist paged me and I immediately went to    |
| the Nuclear Pharmacy laboratory.  I verified that the dose calibrator was    |
| set on I-131and inquired about the package receipt procedures. The Nuclear   |
| Pharmacist indicated that the package was in excellent condition with no     |
| sign of physical damage.  The package was received in a timely manner,       |
| metered and swiped without incident.  The package contained two vials        |
| supposedly containing 140.00 mCi and 14.10 mCi of iodine-131 for a total of  |
| 154.10 mCi.  The contents of the package appeared to be intact.  The Nuclear |
| Pharmacist combined the two vials and assayed the dose in the dose           |
| calibrator for an iodine ablation therapy but measured only 54.0 mCi of      |
| I-131.                                                                       |
|                                                                              |
| "At 11:20 I notified Mallinckrodt of the discrepancy, and then at 11:30 I    |
| notified the NRC Operations Center to report the missing licensed material   |
| in accordance with 10 CFR Part 20.2201(a)(1)(i).  I will also contact the    |
| shipper, MMS Courier, and the Army Medical Command as well as any local or   |
| state notifications that are required."                                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   39842       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 05/12/2003|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 23:08[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        05/12/2003|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        09:00[CDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  05/12/2003|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |SONIA BURGESS        R3      |
|  DOCKET:  0707001                              |MELVYN LEACH         NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  THOMAS WHITE                 |                             |
|  HQ OPS OFFICER:  HOWIE CROUCH                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NBNL                     RESPONSE-BULLETIN      |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| LOSS OF ONE OF TWO CONTROLS ON MODERATION                                    |
|                                                                              |
| NRC BULLETIN 91-01 24 HOUR NOTIFICATION                                      |
|                                                                              |
| The following information was received from the licensee via facsimile:      |
|                                                                              |
| "At 0900 on 5/12/03, the Plant Shift Superintendent (PSS) was notified that  |
| differential pressure transmitter inputs for three Freezer/Sublimers,        |
| U/2(Unit # 2) C/B (Cell B), U3 C/B and U/4 C/B located in C-337, were        |
| installed incorrectly. The transmitter (PDT-338) measures the differential   |
| pressure between the R-114 (freon) and the Recirculating Cooling Water       |
| (RCW). NCSA CAS-001 requires that the pressure differential between the      |
| R-114 and RCW pressures be such that the R-114 pressure is at least 2.0 psia |
| above the RCW pressure. This would preclude the introduction of a moderator  |
| (RCW) into the process side of the system. The correct configuration of      |
| these inputs has the pressure tap on the inlet line to the                   |
| condenser/reboiler. For Freezer/Sublimers U/2 C/B, U/3 C/B and U/4 C/B the   |
| pressure tap is located on the outlet line from the condenser/reboiler.  As  |
| installed, the low differential pressure-alarm may not come in until after   |
| the R-114 pressure and RCW pressure at the inlet of the Condenser/Reboiler   |
| have exceeded the NCS limit.  At 1040 on 5/12/03, the PSS was notified by    |
| Nuclear Criticality Safety that one of the two controls on moderation had    |
| been lost.                                                                   |
|                                                                              |
| The System Engineer identified four additional Freezer/Sublimers, two in     |
| C-331 and two in C-335, with the same problem. These Freezer/Sublimer units  |
| were out-of-service and the RCW had been drained prior to the walk-down. ,   |
|                                                                              |
|                                                                              |
| SAFETY SIGNIFICANCS OF EVENTS:                                               |
|                                                                              |
| Although high side Condenser/Reboiler pressure readings could not be taken   |
| due to incorrect installation of an AQ-NCS pressure instrument, the          |
| integrity of the F/S tubes has been maintained. All of the                   |
| Condenser/Reboilers had the RCW drained by 1345 hours on 5-12-03. thus       |
| re-establishing double contingency.                                          |
|                                                                              |
| POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(s) OF HOW            |
| CRITICALITY COULD OCCUR)                                                     |
|                                                                              |
| In order for a criticality to be possible, an unsafe mass of uranium would   |
| have to be present within the Freezer/Sublimer unit and a moderator would    |
| have to enter through the Freezer/Sublimer and Condenser/Reboiler tubes.     |
|                                                                              |
| CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION,ETC.)       |
|                                                                              |
| Double contingency is maintained by implementing two controls on             |
| moderation.                                                                  |
|                                                                              |
|                                                                              |
| ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS     |
| LIMIT AND  % WORST CASE CRITICAL MASS):                                      |
|                                                                              |
| For the 20 MW Freezer/Sublimers, less than a safe mass of uranium, at less   |
| than or equal to (LEU) U235.                                                 |
| For the 10 MW Freezer/Sublimers, less than a safe mass of uranium, at less   |
| than or equal to (LEU) U235                                                  |
|                                                                              |
|                                                                              |
| NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION   |
| OF THE FAILURES OR DEFICIFNCIES                                              |
|                                                                              |
| The first leg of double contingency relies on Freezer/Sublimer and           |
| Condenser/Reboiler tube integrity. Since high UF6 pressure alarms or other   |
| operational indicators, caused by leaking R-114 into the Freezer/Sublimer,   |
| have not been received on the Freezer/Sublimer units, the integrity of the   |
| Freezer/Sublimer tubes has been maintained. Therefore, this leg of double    |
| contingency was maintained.                                                  |
|                                                                              |
| The second leg of double contingency relies on the differential pressure     |
| between the R-114 and RCW, controlling the differential pressure such that   |
| the R-114 is maintained at least 2.0 psi above the RCW precludes the         |
| introduction of RCW to the process side of the unit. Monitoring the RCW      |
| pressure on the outlet to the Condenser/Reboiler, instead of the inlet, does |
| not give correct differential pressure readings. Therefore. This leg of      |
| double contingency was not maintained.                                       |
|                                                                              |
| Even though the moderation parameter was maintained through integrity of the |
| Freezer/Sublimer and Condenser/Reboiler tubes, double contingency Is based   |
| on two controls on moderation. Thus, double contingency was not maintained.  |
|                                                                              |
| CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLFMENTED:  |
|                                                                              |
| 1. Drain Condenser/Reboiler RCW for the affected Freezer/Sublimer units.     |
| Completed at 1345 on 5-12-03.                                                |
| 2. Correct the installation of the pressure taps In accordance with the      |
| approved Engineering drawings. Complete prior to returning Freezer/Sublimors |
| to service                                                                   |
|                                                                              |
| The NRC Resident Inspector was notified of this event by the licensee.       |
+------------------------------------------------------------------------------+