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McGuire 2
4Q/2008 Plant Inspection Findings


Initiating Events

Significance:a graphic of the significance Dec 31, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Perform an Adequate Risk Assessment for Switchyard Activities
The inspectors identified a NCV of 10CFR50.65(a)(4) for failure to perform an adequate risk assessment for Unit 1 when the performance of switchyard activities affected both units, and were categorized as risk significant for Unit 2. This finding was documented in the licensee’s corrective action program as Problem Investigation Process report (PIP) M-08-6297, and plan to take actions to enhance risk assessment techniques. No immediate corrective action was taken because the work was almost completed by the time the licensee confirmed their error. This finding is greater than minor when compared to IMC 0612 Appendix B, minor question 5(e) because the Unit 1 risk assessment failed to consider maintenance activities that were occurring in the switchyard that affected both units and would have resulted in a higher risk category if properly assessed and could increase the likelihood of initiating events such as loss of offsite power. The finding was determined to be of very low safety significance because the time to boil in the spent fuel pool was slightly over 10 hours, which would have allowed sufficient time such that upon a loss of offsite power there would have been a reasonable likelihood for success of actions taken to recover off-site power. This finding has a cross-cutting aspect of decision making in the area of human performance [H.1.a]. (Section R13)

Inspection Report# : 2008005 (pdf)


Mitigating Systems

Significance:a graphic of the significance Aug 20, 2008
Identified By: NRC
Item Type: VIO Violation
Failure to Take Adequate Corrective Action for Implementation of Safety-Related RN Strainer Backwash
10 CFR 50 Appendix B Criterion XVI, Corrective Action, states that measures shall be
established to assure that conditions adverse to quality, such as deficiencies, deviations,
and non-conformances are promptly identified and corrected. In the case of significant
conditions adverse to quality, the measures shall assure that the cause of the condition
is determined and corrective action taken to preclude repetition. This requirement is
implemented through the Duke Quality Assurance Program Topical Report and
procedure NSD 208, Problem Identification Process.

Contrary to the above, between 2003 and August 7, 2007, the licensee failed to correct a
significant condition adverse to quality related to macro-fouling of the nuclear service
water (RN) strainers, in that the corrective action that was implemented failed to ensure
that the design and licensing basis required capability for manual strainer backwash be
maintained during accident conditions. Specifically, the 2003 plant modification that was
implemented to address macro-fouling (i.e., upgrade and reclassification of the strainer
backwash function to safety-related): (1) utilized non-safety-related instrument air (VI) to
maintain each RN pump=s strainer backwash discharge valve open, but did not provide a
means to manually open (or bypass) the discharge valve to support backwash operations
upon a loss of VI; and (2) did not account for the impact on timely operator response
from higher strainer macro-fouling rates and expected (nuisance) strainer differential
pressure alarms (without fouling) at the onset of high RN flow events (i.e., safety injection
(SI) and loss of VI). As such, there was a lack of reasonable assurance that the RN
system would be able to perform its safety-related function upon a SI or loss of VI event
during periods of macro-fouling.

This violation is associated with a White finding for Units 1 and 2.
Inspection Report# : 2008009 (pdf)

Significance: SL-IV Jun 30, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Update the FSAR to Reflect Those Portions of RN Shared Between Units (Section 1R11.1)
The inspectors identified a non-cited violation of 10 CFR 50.71(e) for the failure to update the Updated Final Safety Analysis Report (UFSAR) to include information related to those portions of the nuclear service water (RN) system that are shared between Units, as reflected in License Amendments issued for both Units on January 4, 1988.

This issue was greater than minor because the failure to include in the UFSAR the designation of which portions of the RN system were shared between units, as described in the License Amendments, was material to the NRC’s review of the licensee’s response to Generic Letter 91-13, Request for Information related to the Resolution of Generic Issue 130, “Essential Service Water System Failures at Multi-Unit Sites.” The licensee’s response revealed that they had procedures that allowed sharing of the RN discharge, which was specifically designated as not shared in Figure 7-1 of the Technical Specifications. As such, the UFSAR could not be relied upon to determine the shared portions and their safety implications. However, the inspectors found no subsequent changes made to the facility that were based on the erroneous information in the UFSAR section. Consequently, this issue was considered to meet the criteria of a severity level IV violation. This finding has a cross-cutting aspect of thorough evaluation in the area of problem identification and resolution [P.1.(c)]. (Section 1R11.1)

Inspection Report# : 2008003 (pdf)

Significance:a graphic of the significance Jun 30, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Scope Main Feedwater Tempering Line Valves Into the Maintenance Rule Monitoring Program (Section 1R12)
The inspectors identified a non-cited violation of 10 CFR 50.65(b)(2)(i) for failure to scope the credited main feedwater tempering lines (one per steam generator) and associated valves into the Maintenance Rule monitoring program.

This finding was more than minor because, similar to Example 7.d of NRC Inspection Manual Chapter (IMC) 0612 Appendix-E, "Examples of Minor Issues," effective control of component condition could not be demonstrated, since the appropriate preventative maintenance was not being performed due to not being
scoped into the Maintenance Rule monitoring program. The licensee satisfactorily tested the functionality of the eight manual valves (two per tempering line) on each unit within the past few years, providing reasonable assurance that the manual valves would operate as required if needed. However, the functionality of the four check valves (one per tempering line) on each unit and the associated flow paths could not be demonstrated at this time; but, the licensee did perform an evaluation of all potential failure mechanisms and determined that the check valves would likely perform their function. The inspectors determined this finding to have very low safety significance, using NRC IMC 0609.04 “Phase 1 Initial Screening,” in that this finding did not represent an actual loss of safety function for equipment designated as risk significant per 10 CFR 50.65, and was not risk significant for external initiating events. (Section 1R12)

Inspection Report# : 2008003 (pdf)

Significance:a graphic of the significance Mar 31, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Establish and Maintain Abnormal Procedures for Loss of Nuclear Service Water (Section 1R11)
The inspectors identified a non-cited violation (NCV) of Technical Specification (TS) 5.4.1.a. for failure to adequately establish and maintain procedures required by Regulatory Guide 1.33, Appendix A, Section 5, Procedures for Abnormal Conditions. Specifically, loss of nuclear service water (RN) procedures were not established and maintained with an adequate safety analysis for the sharing of nuclear service water between units.

This finding is more than minor because it affects the availability, reliability, and capability of the RN system (ultimate heat sink) and is related to the design control and procedure quality attributes of the mitigating systems cornerstone. In addition, this finding could be reasonably viewed as a precursor to a significant event (i.e. loss of RN on both units). The issue was determined to be of very low safety significance in IMC 0609 SDP Phase 1 screening based on the fact that this finding did not represent an actual loss of system safety function nor a loss of a single train of RN for greater than its Technical Specification allowed outage time, because these procedural steps had never been used. This finding has a cross-cutting aspect of resources in the area of human performance [H.2.c] because the licensee failed to ensure that procedures had complete, accurate and up-to-date design documentation to assure nuclear safety. (Section 1R11)

Inspection Report# : 2008002 (pdf)

Significance:a graphic of the significance Mar 31, 2008
Identified By: Self-Revealing
Item Type: NCV NonCited Violation
Failure to Implement Foreign Material Exclusion Control Procedures (Section 1R13)
A self-revealing NCV of TS 5.4.1.a, for failure to adequately implement procedures required by Regulatory Guide 1.33, Appendix A, Section 9, Procedures for Performing Maintenance, was identified. Specifically, foreign material exclusion control procedures as described in work orders were not implemented.

This finding is more than minor because it affects the availability, reliability, and capability of one train of the RN system (ultimate heat sink) and is related to the human performance and procedure quality attributes of the mitigating systems cornerstone. This finding was considered self-revealing because the foreign material (i.e., diver’s knife) was discovered in the 2A RN strainer as a result of the loss of safety equipment functionality. Data related to the frequency of high RN strainer differential pressure alarms was reviewed by the NRC staff for the seasonal macro-fouling periods of 2006 and 2007 to determine the total actual exposure time that macro-fouling occurred. Based on the data, a collective period of less than 30 days was selected as a conservative, bounding exposure number to determine the significance of the collective seasonal macro-fouling for the period from 2006 until January 28, 2008. The issue is of very low safety significance based on review IMC 0609 Appendix A pre-solved risk tables for loss of one train of nuclear service water for less than 30 days. This finding has a cross-cutting aspect of decision making in the area of human performance [H.1.b] because the licensee failed to use conservative assumptions in decision making when deciding not to implement foreign material procedures. (Section 1R13)

Inspection Report# : 2008002 (pdf)

Significance:a graphic of the significance Mar 31, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Nuclear Service Water System Flow Analysis Deficiencies (Section 4OA5.2)
The inspectors identified a NCV of 10 CFR 50, Appendix B, Criterion III, Design Control, for failure to establish measures to verify the design capability of the RN pumps. Specifically, the licensee did not perform system hydraulic analyses or use other means to demonstrate that RN pumps 1A and 1B could perform their safety function under the most limiting design basis conditions.

This finding is more than minor because it affected the design control attribute of the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors assessed the finding using the SDP and determined that the finding was of very low safety significance because subsequent engineering analysis, completed in March 2008, demonstrated there was no loss of RN system safety function capability when the worst case design basis accident (DBA) limiting values were input into the RN system flow analysis. (Section 4OA5.2)

Inspection Report# : 2008002 (pdf)


Barrier Integrity

Significance:a graphic of the significance Jun 30, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Pre-conditioning of Unit 2 MSIVs Prior to Surveillance Testing (Section 1R22)
The inspectors identified a non-cited violation of Technical Specification (TS) 5.4.1.a for failure to establish an adequate procedure to test main steam isolation valves (MSIVs). Specifically, written test control procedures did not prevent and, therefore, resulted in pre-conditioning of the valves prior to their surveillance requirement stroke time testing.

This finding is more than minor because the use of test procedures that allow preconditioning, if left uncorrected, could become a more significant safety concern. Inspection Manual Chapter 9900 Section C.1.c defines pre-conditioning as the alteration, variation, manipulation, or adjustment, of the physical condition of structures, systems and components (SSCs) before TS surveillance or ASME code testing. Pre-conditioning can affect the acceptability of test results and can have a direct effect on the determination of operability of the affected system or component by masking the true as-found condition. As such, this issue also affects the barrier integrity cornerstone objective of maintaining containment functionality and the associated attributes of SSC barrier performance, and procedure quality, by affecting the determination of operability related to the containment isolation function of the MSIVs. This issue is of very low safety significance because there was insufficient information to show that the MSIVs were inoperable during the short period of time that they were required in Modes 3, 2 and 1; therefore, it did not represent an actual open pathway in the physical integrity of the containment. This finding has a cross-cutting aspect of decision making in the area of human performance [H.1.(b)]. (Section 1R22)

Inspection Report# : 2008003 (pdf)


Emergency Preparedness


Occupational Radiation Safety

Significance: SL-IV Dec 31, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Control a Locked-High Radiation Area Barrier [EA-08-268]
The inspectors identified a NCV of Technical Specification (TS) 5.7.2 for the licensee’s failure to control access to a locked-high radiation area (LHRA). Specifically, on September 30, 2006, a contract radiation protection technician (RPT) left the reactor head inspection stand LHRA barrier unlocked and unguarded from approximately 5:05 to 5:21 a.m. Dose rates as high as 10 rad/hr at 30 cm and 4 rad/hr general area were present inside the reactor head stand LHRA. The significance of the violation was assessed using traditional enforcement because it involved willfulness [EA-08-268]. In accordance with Supplement IV, Health Physics, of the NRC Enforcement Policy, the NRC determined that the safety significance of this violation was SL IV because the situation described in example 7 of a SL III violation (the finding involves a situation with a substantial potential for exposure in excess of applicable limits) did not exist and, per example 9 of a SL IV violation, was a matter with more than a minor safety, health, or environmental significance. Although this violation involved willfulness, it was dispositioned as an NCV in accordance with Section IV.A.1 of the Enforcement Policy because the licensee identified the violation and promptly discussed it with regional health physics inspectors, the violation involved the acts of a low-level individual, the violation appears to be the isolated action of the employee without management involvement, and significant remedial action commensurate with the circumstances was taken by the licensee. The finding was documented in the licensee’s corrective action program as PIP M-06-4479. (Section 4OA5.2)

Inspection Report# : 2008005 (pdf)


Public Radiation Safety


Physical Protection

Although the NRC is actively overseeing the Security cornerstone, the Commission has decided that certain findings pertaining to security cornerstone will not be publicly available to ensure that potentially useful information is not provided to a possible adversary. Therefore, the cover letters to security inspection reports may be viewed.


Miscellaneous

Significance: N/A Aug 29, 2008
Identified By: NRC
Item Type: FIN Finding
McGuire PI&R
The team concluded that, in general, problems were properly identified, evaluated,
prioritized, and corrected. The licensee was effective at identifying problems and
entering them into the corrective action program (CAP) for resolution. The licensee
maintained a low threshold for identifying problems as evidenced by the large number of
Problem Investigation Process reports (PIPs) entered annually into the CAP. Generally,
the licensee properly prioritized and evaluated issues, formal root cause evaluations for
significant problems were thorough and detailed, and corrective actions specified for
problems were adequate. Overall, corrective actions developed and implemented for
issues were effective in correcting the problems. However, the team identified examples
where reportability issues were not dispositioned in a timely manner, root causes were
not adequately identified, and corrective actions were not focused to correct problems.

The team determined that audits and self-assessments were effective in identifying
deficiencies and areas for improvement in the CAP, and in most cases, corrective
actions were developed to address these issues. Operating experience usage was
found to be effective and well integrated into the licensee’s processes for performing and
managing work, and plant operations. Personnel at the site felt free to raise safety
concerns to management and use the CAP to resolve.
Inspection Report# : 2008006 (pdf)

Last modified : January 30, 2009